N407FJ

DORNIER 328-300 · 2000 · Valid Registration

Registered owner: ULTIMATE LEASING LLC, OH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Ultimate JETCHARTERS, LLC (DTHA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2008-02-11 Matched by certificate designator
ATA 2133

EN ROUTE DTW TO CLT AT FL310 UNCOMMANDED CABIN ALTITUDE CLIMB TO 9100'. MAINTENANCE DETERMINED PNEUMATIC OUTFLOW VALVE/FILTER ASSY CONTAMINATED. VALVE AND FILTERS CLEANED, FUNCTION RESTORED.

Source: SDR DTHA2008001 · FAA SDRS
O · 2006-04-26 Matched by certificate designator
ATA 3160

THE NR 1 MFD DISPLAY UNIT REFERENCED HERE IN FAILED DURING TAXI OPERATIONS PRIOR TO FLIGHT. THE SUSPECTED SPECIFIC COMPONENT FAILURE IS THE HIGH VOLTAGE POWER SUPPLY UNIT PN:7018704-902 INSTALLED INSIDE THE CRT DISPLAY UNIT. FURTHER INSPECTIONS WILL BE REQUIRED TO VERIFY THE EXACT CAUSE OF DU FAILURE.

Source: SDR CMRR200604011 · FAA SDRS
O · 2006-04-26 Matched by certificate designator
ATA 3160

THE NR 1 PFD DISPLAY UNIT REFERENCED HERE IN FAILED DURING TAXI OPERATIONS PRIOR TO FLIGHT. THE SUSPECTED SPECIFIC COMPONENT FAILURE IS THE HIGH VOLTAGE POWER SUPPLY UNIT PN:7018704-902 INSTALLED INSIDE THE CRT DISPLAY UNIT. FURTHER INSPECTIONS WILL BE REQUIRED TO VERIFY THE EXACT CAUSE OF DU FAILURE.

Source: SDR CMRR200604010 · FAA SDRS
J · 2004-08-01 Matched by certificate designator
ATA 7314

LOW SPEED ABORT DUE TO LOW FUEL PRESSURE MESSAGE. FOUND LEFT JET PUMP SWITCH PUSHED.

Source: SDR 04214407 · FAA SDRS
L · 2003-10-10 Matched by certificate designator
ATA 3350

DURING INSPECTION THE EMERGENCY LIGHTS NEAR SEATS 4 AND 5 B AND C WERE FOUND INOPERATIVE. MAINTENANCE PERSONNEL REMOVED AND REPLACED THE EMERGENCY POWER SUPPLY. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RELEASED FOR CONTINUED SERVICE.

Source: SDR 03283407 · FAA SDRS
B · 2003-01-31 Matched by certificate designator
ATA 2120

AFTER TAKE OFF, CREW REPORTED HEAVY SMOKE IN COCKPIT. AN EMERGENCY WAS DECLARED WITH ATC AND AIRCRAFT RETURNED TO POINT OF DEPARTURE. AIRCRAFT LANDED WITHOUT ANY FURTHER INCIDENT. MAINTENANCE PERSONNEL INSPECTED AND ADJUSTED CROSSBLEED VALVE AND RAN ENGINES, NO SMOKE NOTED. AN OPERATIONAL CHECK WAS SATISFACTORY AND THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR 03031407 · FAA SDRS
E J · 2002-02-04 Matched by certificate designator
ATA 2435

DURING CRUISE FROM CHS TO LGA RT ENGINE VIBRATION ICON ILLUMINATED INDICATING VIBRATIONS >.2" UP TO 1.3" PER SECOND. FLIGHT CREW COMPLIED WITH QRH AND DIVERTED TO PHL. AN EMERGENCY WAS DECLARED WITH ATC AND A/C LANDED IN PHL WITHOUT FURTHER INCIDENT. MAINTENANCE PERSONNEL REMOVED AND REPLACED STARTER GENERATOR AND PERFORMED HIGH ENGINE RUNS, NO FURTHER DEFECTS NOTED AND ALL INDICATIONS WERE WITHIN LIMITS. AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR 02035407 · FAA SDRS