N408GJ

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
GJ COMPANY HOLDINGS, LLC (MFGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

S · 2022-04-12 Matched by certificate designator
ATA 3400

DURING DEPARTURE FROM KAPF THE CREW WERE FLYING TO CSHELL FIX AND WERE NOTIFIED BY ATC THE WERE 50 MILES OFF COURSE WITH ALL COCKPIT NAVIGATION INDICATIONS NORMAL. THE CREW THEN ELECTED TO RETURN TO KAPF VIA ATC VECTORING AND LANDED WITH OUT ISSUE. MAINTENANCE WAS DISPATCHED TO THE AIRCRAFT AND FOUND BOTH FMS'S AND GPS'S NOT SYNCED.AFTER PERFORMING SYNCING PROCEDURE PER 400A AMM 34-20-01 SYSTEMS SHOWED NO ERRORS. THE AIRCRAFT WAS RETURNED TO SERVICE AND HAS FLOWN WITH OUT ANY OTHER ISSUES.

Source: SDR MFGA20220412001 · FAA SDRS
O · 2021-07-01 Matched by certificate designator
ATA 7603

CREW REPORTED LEFT HAND ENGINE POWER LEVER FROZE AT 80% N1 ON DESCENT INTO MARSH HARBOR BAHAMAS, AS A PRECAUTIONARY MEASURE THE CREW ELECTED TO DIVERT TO MYNN. BIG SKY AVIATION CRS# 4B1R824C WAS CONTACTED AND THEY DISPATCHED A&P 2640501 DEXTER ADDERLEY. UPON INSPECTION OF THE LEFT HAND ENGINE THROTTLE CABLE A FEW CLAMPS WERE FOUND NOT SECURED ALLOWING BINDING OF THE CABLE. CLAMPS WERE SECURED AND FULL FREEDOM OF MOVEMENT WAS RESTORED TO THE LEFT ENGINE POWER CONTROL SYSTEM. THE AIRCRAFT HAS NOT REPORTED THE ISSUE AGAIN.

Source: SDR MFGA2021F00074 · FAA SDRS