N417TS

DIAMOND AIRCRAFT IND INC DA 42 · 2006 · Valid Registration

Registered owner: NYMOON LLC, CA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

F · 2017-05-09 Matched by certificate designator
ATA 6123

DURING A ROUTINE PART 61 TRAINING FLIGHT, THE RIGHT ENGINE WAS INTENTIONALLY SHUTDOWN TO DEMONSTRATE INFLIGHT RESTARTS. AFTER A NORMAL SHUTDOWN AND SECURING PROCEDURE, THE ENGINE MASTER SWITCH WAS SWITCHED BACK TO THE ON IAW THE CHECKLIST. USUALLY THIS WOULD DRIVE THE PROPELLER OUT OF FEATHER, AND THE RESTART PROCEDURE COULD BE CONTINUED. THE CFI NOTICED THAT THE PROPELLER DID NOT UNFEATHER, AND THEY ATTEMPTED SEVERAL TROUBLESHOOTING PROCEDURES. IT WAS THEN DECIDED TO RETURN TO DEPARTURE UTILIZING A SINGLE-ENGINE. AFTER TROUBLESHOOTING THE PROPELLER ISSUE, IT WAS DETERMINED THAT THE GOVERNOR WAS "STICKING" AND NOT ALLOWING THE PROP TO MOVE FROM FEATHER. THE GOVERNOR WAS REPLACED WITH NEW UNIT. ALL OPS CHECKS WERE NORMAL AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR B90A20170509001 · FAA SDRS
F · 2017-05-09 Unresolved
ATA 6123

DURING A ROUTINE PART 61 TRAINING FLIGHT, THE RIGHT ENGINE WAS INTENTIONALLY SHUTDOWN TO DEMONSTRATE INFLIGHT RESTARTS. AFTER A NORMAL SHUTDOWN AND SECURING PROCEDURE, THE ENGINE MASTER SWITCH WAS SWITCHED BACK TO THE ON IAW THE CHECKLIST. USUALLY THIS WOULD DRIVE THE PROPELLER OUT OF FEATHER, AND THE RESTART PROCEDURE COULD BE CONTINUED. THE CFI NOTICED THAT THE PROPELLER DID NOT UNFEATHER, AND THEY ATTEMPTED SEVERAL TROUBLESHOOTING PROCEDURES. IT WAS THEN DECIDED TO RETURN TO DEPARTURE UTILIZING A SINGLE-ENGINE.

Source: SDR 2017FA0000179 · FAA SDRS
R · 2017-03-01 Unresolved
ATA 6100

DURING THE INITIAL TAKEOFF ROLL, THE LEFT PROPELLER DID NOT RESPOND TO THROTTLE APPLICATION. MAINTENANCE FOUND TORSION VIBRATION DAMPENER HUB BROKEN, WHICH DISCONNECTED ENGINE TO GEARBOX DRIVE TRAIN CONNECTION. TVD WAS ALSO FOUND CRACKED, CONTAMINATION IN GEARBOX, AND PROPELLER GOVERNOR SEIZING DUE TO SUSPECTED GEARBOX CONTAMINATION. TVD, TVD HUB, GEARBOX, AND PROP GOVERNOR REPLACED.

Source: SDR 2017F00090 · FAA SDRS