N490SA

TEXTRON AVIATION INC 208B · 2026 · Valid Registration

Registered owner: TVPX AIRCRAFT SOLUTIONS INC TRUSTEE, UT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
SUMMIT HELICOPTERS, INC. (BHHA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 1999-01-19 Matched by certificate designator
ATA 5720

DURING CHECK-C MAINT, FOUND ONE INCH CRACK IN LT WING IN UPPER WING FUEL TANK ACCESS PLATE DOUBLER NR 1307. STOP DRILLED CRACK AND INSTALLED REPAIR PER SRM 57-03 AND SRM 51-60-0.

Source: SDR TWAA9901308 · FAA SDRS
O · 1999-01-12 Matched by certificate designator
ATA 5330

DURING CHECK-C MAINT CHECK, FOUND SIX INCH CRACK IN FUSELAGE SKIN AT STA 514, 12 IN BELOW OVERWING EXIT OPENING ON LEFT SIDE OF AIRCRAFT. REPAIRED CRACK PER ARA 15854 AND ARA 15856.

Source: SDR TWAA9900902 · FAA SDRS
B · 1998-09-16 Matched by certificate designator
ATA 7200

SHORTLY AFTER TAKEOFF, SMELLED INITIAL ODOR IN COCKPIT AND CABIN. RESEMBLED BURNING IN OVENS BUT MORE ACRID. LATER DESCRIBED AS CHEMICAL ELECTRICAL SMELL. FLT RETURNED TO STL. FOUND BIRD HAD BEEN INJESTED IN LT ENGINE AFFECTING THE PNEUMATIC SYSTEM. ACCOMPLISHED BIRD STRIKE INSPECTION. NO DAMAGE TO ENGINE. CHECK-C 9-5-97 STL. (X)

Source: SDR TWAA9815101 · FAA SDRS
J · 1997-08-23 Matched by certificate designator
ATA 7510

MCI - FLT 477 - DURING CLIMB, THE NR 2 ENGINE, FUEL HEAT VALVE STUCK IN THE OPEN POSITION CAUSING HIGH ENGINE OIL TEMPERATURE. SHUT DOWN ENGINE. REMOVED AND REPLACED THE FUEL HEAT VALVE, MFG P/N 3201115, MANUFACTURED BY WHITTAKER CONTROLS. OPERATIONAL CHECK AND ENGINE RUNS NORMAL. (M)

Source: SDR TWAA9799004 · FAA SDRS
K J · 1996-12-23 Matched by certificate designator
ATA 7930

STL - DURING CRUISE, SHUT DOWN NR 2 ENGINE, S/N 3811, DUE TO LOSS OF OIL QTY. FOUND OIL FILTER BYPASS SWITCH, MFG P/N 42D109-1A, LEAKING. REPLACED OIL FILTER BYPASS SWITCH. ENGINE OPERATION AND LEAKS CHECKS NORMAL. (M)

Source: SDR TWAA9616001 · FAA SDRS
P · 1996-11-17 Matched by certificate designator
ATA 3260

STL - FLT 483 - DURING APPROACH WHEN LANDING GEAR WAS EXTENDED, LANDING GEAR DID NOT SHOW DOWN AND LOCKED. FOUND LANDING GEAR INDICATOR LAMP, MFG PN MS25231-313, SHORTING OUT INDICATOR SOCKET, MFG PN 035-1881-007. RELAMPED INDICATOR AND RESET P26 CIRCUIT BREAKER. LANDING GEAR INDICATION THEN CHECKED NORMAL. CHECK C - 7-11-96 - STL. (X)

Source: SDR TWAA9614001 · FAA SDRS
O · 1996-07-02 Matched by certificate designator
ATA 5210

STL - DURING OP-15, FOUND .25 INCH CRACK IN FORWARD LOWER DOOR BEAM FITTING RIVET HOLE. REPAIRED PER SRM 51-00 AND TWA STANDARD PRACTICES. AIRCRAFT TOTAL TIME 63,299, AIRCRAFT TOTAL CYCLES 77,392.

Source: SDR 96ZZZM1217 · FAA SDRS
J · 1996-04-08 Matched by certificate designator
ATA 3231

STL - FLT 692 - AFTER TAKEOFF FOLLOWING GEAR RETRACTION, THE RT MAIN GEAR UNSAFE LIGHT REMAINED ON. ADJUSTED RT MAIN GEAR DOOR LATCH ASSY. PERFORMED GEAR SWING, OPERATION NORMAL. CHECK C - 2-17-95 - MCI. (X)

Source: SDR 96ZZZX2130 · FAA SDRS
B · 1995-12-10 Matched by certificate designator
ATA 2530

CID - FLT 64 - DURING CRUISE, FIRST CLASS COFFEEMAKER EMITTED SMOKE. TURNED OFF COFFEEMAKER AND OPENED CIRCUIT BREAKER. FOUND INTERNAL MALFUNCTION IN COFFEEMAKER. REPLACED COFFEEMAKER, MFG PN 50198A, AND OPERATION CHECKED NORMAL. CHECK C - 2-17-95 - MCI.

Source: SDR 96ZZZX646 · FAA SDRS