N496JH

CESSNA 560 · 1998 · Valid Registration

Registered owner: N496JH LLC, NM (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
RED WING AEROPLANE, LLC. (R3WA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

M B J · 2021-02-04 Matched by certificate designator
ATA 2100

AT 40000 FEET THE EMERGENCY PRESSURIZATION CAME ON FULL WITH THE SWITCH OFF. CREW IMMEDIATELY CHECKED THE CABIN ALTITUDE AND FOR ANY RATE OF DESCENT OF THE PRESSURIZATION. ALL LOOKED STABLE, THEN THE EMERG PRESS ON LIGHT CAME ON WITH A SLIGHT SMELL OF SMOKE IN THE CABIN. PILOT DECLARED AN EMERGENCY AND ASKED FOR AN EMERGENCY DESCENT AND ATC GAVE ME 25000. DURING THE DESCENT THE CABIN DESCENDED NORMALLY. WE ACCOMPLISHED THE EMERGENCY CHECKLIST AND THE SYSTEM RESET. SINCE EVERYTHING WAS LOOKING NORMAL I CANCELED THE EMERGENCY AND STAYED AT 25000 FOR FUEL. ABOUT 10 MINUTES LATER LATER IT ALL HAPPENED AGAIN AND WOULD NOT RESET SO I DECLARED AND EMERGENCY AND RAPID DESCENDED TO 4000 FEET, WENT STRAIGHT TO THE AIRPORT AND LANDED ON RUNWAY 14 AND TAXIED TO ATLANTIC. ACM WAS LATER DEFERRED AND AIRCRAFT FLOWN TO KMCO FOR MAINTENANCE. MAINTENANCE FOUND ERRATIC OHMS IN THE 450 DEGREE SWITCH IN THE ACM.

Source: SDR R3WA202102230001 · FAA SDRS
K J · 2018-10-23 Matched by certificate designator
ATA 3240

AFTER CREW LOWERED MAIN LANDING GEAR, POWER BRAKE ANNUNCIATION LIGHTS ILLUMINATED. CREW REQUESTED A GO AROUND TO CHECK ISSUE AND RUN CHECKLIST. CREW REQUESTED LONGER RUNWAY AND LANDED WITH LOW BRAKE PRESSURE. CREW USED REVERSE THRUSTER TO SLOW AIRCRAFT AND EXITED RUNWAY AND STOPPED ON TAXIWAY. FBO TOWED AIRCRAFT IN. TECH IN KOMA WAS CONTACTED TO TROUBLESHOOT ISSUE. FLUID WAS FOUND IN LEFT GEARWELL AND BRAKE RESERVOIR EMPTY. BRAKE RESERVOIR WAS SERVICED AND BRAKE SYSTEM OPS CHECKED. MAINTENANCE FOUND A LEAKING LEFT BRAKE LINE DUE TO SWEDGING FAILURE AT COUPLING NUT. NEW BRAKE LINE WAS ORDERED FROM AND LINE WAS REPLACED THE FOLLOWING DAY. BRAKE SYSTEM WAS CLEANED OUT, SERVICED, AND BLED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR R3WA2019F00096 · FAA SDRS