N499CZ

BEECH 99A · 1969 · Valid Registration

Registered owner: N499CZ LLC, WI (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FREIGHT RUNNERS EXPRESS, INC. (KCQA)Certificate holderMatched by certificate designator
FREIGHT RUNNERS EXPRESS, INC. (KCQA)Operator2020-10-14 – 2020-10-14Operator named in NTSB report
Freight RunnersOperator2020-10-14 – 2020-10-14Operator named in NTSB report

Accident & incident history

Acc · 2020-10-14 Operator named in NTSB report
BEECH 99 None injury Part 135Freight Runners
Source: NTSB case ERA21LA021

Maintenance disclosures

N · 2024-10-23 Matched by certificate designator
ATA 2612

RIGHT ENGINE T-HANDLE ILLUMINATED THEN WENT OUT FOLLOWED BY AGGRESSIVE ENGINE SURGING. EXECUTED ENGINE SHUTDOWN AND LANDED. FOUND NO EVIDENCE OF ANY FIRE ON THE RH ENGINE AND TESTED THE FIRE DETECTOR SYSTEM MORE THAN 5 DIFFERENT TIMES, COULD NOT DUPLICATE PROBLEM AND NO DEFECTS FOUND AT THIS TIME. REPLACED PROP GOVERNOR IAW BE 99 MM 61-20-00 OPS CHECKED AND LEAK CHECKED GOOD NO DEFECTS FOUND AT THIS TIME.

Source: SDR 2024F00262 · FAA SDRS
K · 2023-06-04 Matched by certificate designator
ATA 3243

PILOT RH HAND BRAKE INOPERATIVE. ON WO# 000101 DATED 06/05/2023 FOUND EMPTY BRAKE RESERVOIR. INSPECTED BRAKE PLUMBING AND FOUND LEAKING LOWER HOSE ON PILOT SIDE RH MASTER CYLINDER. REMOVED AND REPLACED WITH NEW HOSE AND BLED BRAKES IAW BE99 AMM 32-40-00 AND BE99 AAIP. OPS AND LEAKS CHECKS GOOD.

Source: SDR KCQA202306050504 · FAA SDRS
K · 2023-06-04 Matched by certificate designator
ATA 2910

ON TAXI THE PILOT FOUND THE RH HAND BRAKE INOPERATIVE. ON FRE/ACE WORK ORDER 000101 DATED 06/05/2023 THE AMT FOUND AN EMPTY BRAKE RESERVOIR. INSPECTED BRAKE PLUMBING AND FOUND LEAKING LOWER HOSE ON PILOT SIDE RH MASTER CYLINDER. REMOVED AND REPLACED WITH NEW HOSE PN MS28741-4-0132 SN NSN AND BLED BRAKES IAW BE99 AMM 32-40-00 AND BE99 AAIP. OPS AND LEAKS CHECKS GOOD. N499CZ HAS BEEN RETURNED BACK TO SERVICE.

Source: SDR KCQA202306070004 · FAA SDRS
Z · 2022-06-20 Matched by certificate designator
ATA 3210

LH MLG DRAG BRACE ATTACH FITTING PN 50-120201-1 CRACKED. REMOVED AND REPLACED COMPLETE LH DRAG BRACE SUPPORT ASSEMBLY PN 50-120202-601. WORK PERFORMED IAW SIRM 20-00-00 AND 20-50-00.

Source: SDR KCQA20220620 · FAA SDRS
K · 2021-11-29 Matched by certificate designator
ATA 3200

WHILE TAXING THE AIRCRAFT AFTER LANDING THE FLIGHT CREW NOTICED THERE WAS A LOSS OF BRAKING ON THE LH SIDE. FOUND LEAKING BRAKE FLUID OUT OF THE LH BRAKE LINE WHERE IT GOES TO THE CALIPER. TIGHTENED THE BRAKE LINE GOING INTO THE LH OUTBOARD CALIPER. BLED THE BRAKES AND LEAK CHECKED GOOD IN ACCORDANCE WITH THE BEECHCRAFT 99 MAINTENANCE MANUAL. NO DEFECTS FOUND AT THIS TIME. NO FURTHER ACTION IS REQUIRED.

Source: SDR KCQA20211207 · FAA SDRS
Z · 2020-10-14 Matched by certificate designator
ATA 3211

DURING LANDING RT MAIN LANDING GEAR DRAG LEG FITTING FAILED.

Source: SDR 2021F00000 · FAA SDRS
N · 2018-09-04 Matched by certificate designator
ATA 2612

IN FLIGHT PILOT RECEIVE FIRE INDICATION ON NR 1 ENGINE. ENGINE SHUTDOWN IAW EMERGENCY PROCEDURES. DURING EXAMINATION OF ENGINE AND NACELLE NO EVIDENCE OF FIRE WAS PRESENT.

Source: SDR KCQA2018090400001 · FAA SDRS
O · 1999-04-12 Matched by certificate designator
ATA 2612

FOUND FIREWALL CONNECTOR TO BE WET WITH WATER. PILOT REPORTED FLYING THROUGH SOME INTENSE SHOWERS EN ROUTE TO MILWAUKEE, WI FROM STEVENS POINT, WI. CONNECTOR WAS DRIED OUT, RE-ASSEMBLED, AND FUNCTION TESTED SATISFACTORY.

Source: SDR 99ZZZX1916 · FAA SDRS
O · 1998-01-13 Matched by certificate designator
ATA 7320

ENGINE POWER WOULD NOT DECREASE DUE TO TIGHT ROD END CONNECTOR FROM CAM BOX TO FCU DEFECTIVE. TAT: 30,824 HOURS. ENGINE TSN: 4,295 HOURS. ENGINE TSO: 1,129 HOURS.

Source: SDR 98ZZZX534 · FAA SDRS
O · 1998-01-13 Matched by certificate designator
ATA 7320

ENGIEN POWER WOULD NOT DECREASE DUE TO BINDING ROD END CONNECTOR CAM BOX TO FCU. TAT: 30,824 HOURS. ENG TSN: 4,295 HOURS. ENG TSO: 1,129 HOURS.

Source: SDR 98ZZZX2711 · FAA SDRS