N500PH

MCDONNELL DOUGLAS HELICOPTER 369E · Valid Registration

Registered owner: PRECISION HELI-SUPPORT LLC, AZ (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Paradise HelicoptersOperator2013-07-25 – 2013-07-25Operator named in NTSB report

Accident & incident history

Acc · 2013-07-25 Operator named in NTSB report
MCDONNELL DOUGLAS HELICOPTER 369E None injury Part 135Paradise Helicopters
Source: NTSB case WPR13CA342

Maintenance disclosures

F · 2011-10-23 Matched by certificate designator
ATA 2730

ELECTRICAL TRIM FAILURE IN FLIGHT RESULTING IN A FULL RT DEFLECTION ON THE TRIM ACTUATOR. PRECAUTIONARY LANDING CONDUCTED AT AIRPORT OF ORIGIN. ACFT TOWED TO MX FACILITY. INSPECTION REVEALED THAT THE TRIM SWITCH LOCATED ON THE CYCLIC HAD BECOME STUCK IN THE FULL RT POSITION RESULTING IN TRIM MOTOR ACTIVATION TO FULL RIGHT. REPLACED TRIM SWITCH WITH SERVICEABLE PART.

Source: SDR K2DA2012F00002 · FAA SDRS
E · 2011-08-23 Matched by certificate designator
ATA 6510

PILOT NOTICED A VIBRATION & METAL ON METAL BANGING NOISE WHEN ACCELERATING FROM GROUND IDLE TO FLT IDLE. PERFORMED EMERGENCY SHUTDOWN & NOTICED TAIL ROTOR APPEARED TO BE TURNING INDEPENDENT OF MAIN ROTOR. INSPECTION REVEALED THE T/R DRIVE SHAFT HAD SHEARED AT AFT END OF PLENUM TUBE. UPON TEARDOWN, DISCOVERED SPOT WELDS ON THE AFT SUPPORT OF T/R DRIVE SHAFT HAD BROKEN, ALLOWING SHAFT TO CONTACT TUBE. DRIVE SHAFT TUBE REPLACED. AFTER REPAIRS & DURING BALANCING TAIL ROTOR, FOUND ELASTOMERIC BEARINGS IN T/R FORK ASSY CAUSED OUT OF LIMITS VIBRATION. T/R FORK ASSY REPLACED. TAIL ROTOR BALANCED & AIRCRAFT RETURNED TO SERVICE.

Source: SDR K2DA20110823001 · FAA SDRS
R J · 2010-03-04 Matched by certificate designator
ATA 7532

PILOT NOTED LOW POWER AND HIGH TOT. DURING CRUISE FLIGHT.

Source: SDR 2010F00067 · FAA SDRS
K · 2008-08-06 Matched by certificate designator
ATA 7320

ON OR AROUND 5:00 PM, WEDNESDAY, 6 AUGUST, 2008, WHILE CONDUCTING A POST FLIGHT INSP, DISCOVERED SOME OIL LEAKAGE IN ENGINE COMPARTMENT. AS HE WAS INVESTIGATING LEAKAGE, NOTICED THAT THE FUEL FILTER PRESSURE SWITCH HAD PLAYED BETWEEN TWO BODY HALVES AND HAD SOME FUEL LEAKAGE. AT WHICH TIME, GROUNDED HELICOPTER, RESCHEDULED OUR FLIGHTS FOR NEXT DAY, AND ORDERED THE PART TO REPAIR THE FAULT. AT THIS TIME, HAVE NO PROBABLE CAUSE FOR THIS INCIDENT BUT DID INFORM THE MECHANIC TO USE CAUTION IN TORQUING THE LINES AND FITTINGS THAT CONNECT THIS PART TO THE ENGINE. (K)

Source: SDR K2D2008F00000 · FAA SDRS
K · 1999-11-17 Matched by certificate designator
ATA 2822

GREASE LEAKING FROM DRAIN.

Source: SDR HEEA065197 · FAA SDRS
O · 1999-04-05 Matched by certificate designator
ATA 2435

STARTER/GENERATOR WILL NOT CRANK ENGINE.

Source: SDR HEEA061680 · FAA SDRS
B R · 1998-11-03 Matched by certificate designator
ATA 7200

SHORTLY AFTER TAKEOFF, PILOT REPORTED 'SMALL EXPLOSION' WITH SPARKS AND 'SMOKE' FROM THE RT ENGINE. SECURED SAME AND RETURNED TO AIRPORT AND MADE UNEVENTFUL SINGLE ENGINE LANDING. MAINTENANCE FOUND N1 SECTION OF ENGINE LOCKED UP. NII SECTION FREE TO ROTATE.

Source: SDR 98ZZZX4612 · FAA SDRS
O · 1998-08-17 Matched by certificate designator
ATA 3421

ARTIFICAL HORIZON SLOW TO ERECT.

Source: SDR HEEA0015642 · FAA SDRS
O · 1998-06-22 Matched by certificate designator
ATA 2211

DESCENDS BEYOND THE SELECTED ALTITUDE OVER CORRECTING IN BANK. TIME SINCE REPAIR 308:00 HOURS.

Source: SDR HEEA0014878 · FAA SDRS
O · 1998-06-22 Matched by certificate designator
ATA 3710

VACUUM SYSTEM VALVE INOPERATIVE.

Source: SDR HEEA0014879 · FAA SDRS
O · 1998-06-04 Matched by certificate designator
ATA 3452

ALTITUDE SELECT FUNCTION IS INOPERATIVE.

Source: SDR HEEA0014552 · FAA SDRS
O · 1998-06-02 Matched by certificate designator
ATA 2140

HEATER BLOWER INOPERATIVE.

Source: SDR HEEA0014467 · FAA SDRS
O · 1998-05-01 Matched by certificate designator
ATA 3441

RNAV PROCESSOR UNIT HAS SOME SEGMENTS THAT ARE INOPERATIVE.

Source: SDR HEEA0014101 · FAA SDRS
O · 1998-03-26 Matched by certificate designator
ATA 3451

DME WILL NOT RECEIVE ON 110 FREQUENCIES.

Source: SDR HEEA0013601 · FAA SDRS
O · 1998-03-26 Matched by certificate designator
ATA 2562

REMOVED WITH CVR S/N 288 FOR WILL NOT TEST IN AIRCRAFT.

Source: SDR HEEA0013622 · FAA SDRS
L · 1998-03-26 Matched by certificate designator
ATA 2370

CVR WILL NOT TEST IN AIRCRAFT.

Source: SDR HEEA0013621 · FAA SDRS
O · 1998-03-19 Matched by certificate designator
ATA 3422

GYRO COMPASS SLOW TO SLAVE.

Source: SDR HEEA0013467 · FAA SDRS
O · 1998-01-07 Matched by certificate designator
ATA 7230

RIGHT ENGINE FAILED SHORTLY AFTER TAKEOFF. LABRATORY REPORT FROM P & W CONTRIBUTED ENGINE FAILURE TO 1ST STAGE COMPRESSOR STATOR FAILURE. STATOR AIRFOIL FAILED DUE TO HIGH CYCLE FATIGUE.

Source: SDR 99ZZZX390 · FAA SDRS
K · 1997-12-03 Matched by certificate designator
ATA 2810

FUEL CELL LEAKING.

Source: SDR HEEA0012204 · FAA SDRS
O · 1997-11-28 Matched by certificate designator
ATA 3233

NLG ACTUATOR EXCESSIVE END PLAY.

Source: SDR HEEA0012152 · FAA SDRS
O · 1997-11-10 Matched by certificate designator
ATA 3451

DME INDICATOR FLASHES INTERMITTENTLY.

Source: SDR HEEA0011885 · FAA SDRS
O · 1997-10-22 Matched by certificate designator
ATA 7712

CALIBRATION IS OFF, TORQUEMETER TRANSMITS HIGH.

Source: SDR HEEA0011719 · FAA SDRS
O · 1997-04-16 Matched by certificate designator
ATA 3442

INOPERATIVE, BUTTONS WON'T LIGHT AND SCREEN BLANK.

Source: SDR HAIHEEA9392 · FAA SDRS
O · 1997-02-10 Matched by certificate designator
ATA 2841

INACCURATE FUEL QTY READING THROUGHOUT RANGE.

Source: SDR HEEA978988 · FAA SDRS
O · 1997-01-14 Matched by certificate designator
ATA 2312

TRANSCEIVER VERY WEAK. TIME SINCE REPAIR 278:50.

Source: SDR HEEA978880 · FAA SDRS
O · 1996-10-14 Matched by certificate designator
ATA 7722

INDICATOR STICKS AT 600 DEGREES.

Source: SDR HEEA968313 · FAA SDRS
O · 1996-10-14 Matched by certificate designator
ATA 7700

INDICATOR READS HIGH; CANNOT ADJUST.

Source: SDR HEEA968314 · FAA SDRS
O · 1996-06-04 Matched by certificate designator
ATA 3442

RADAR INTERMITTENT.

Source: SDR HEEA967319 · FAA SDRS
O · 1996-04-08 Matched by certificate designator
ATA 3421

GYRO INTERMITTENT SIGNAL.

Source: SDR HEEA966957 · FAA SDRS
O · 1995-09-12 Matched by certificate designator
ATA 7931

TRANSMITTER FAILED.

Source: SDR HEEA955718 · FAA SDRS
O · 1995-07-24 Matched by certificate designator
ATA 6111

DAMAGE TO ONE BLADE TIP. TSO DUE 9-97.

Source: SDR HEEA955430 · FAA SDRS
O · 1995-04-24 Matched by certificate designator
ATA 2211

YAW DAMPER INOPERATIVE. TIME SINCE REPAIR 1284:40.

Source: SDR HEEA954848 · FAA SDRS
O · 1995-03-22 Matched by certificate designator
ATA 2210

CAUSES YAW DAMPER TO SWING SIDE TO SIDE.

Source: SDR HEEA954576 · FAA SDRS
O · 1995-02-14 Matched by certificate designator
ATA 3420

WILL NOT RUN CO-PILOTS HSI. GIVES WRONG SIGNAL. TIME SINCE REPAIR 1298:25.

Source: SDR HEEA954350 · FAA SDRS
L · 1995-02-10 Matched by certificate designator
ATA 2370

CVR WILL NOT TEST.

Source: SDR HEEA954337 · FAA SDRS