N500UP

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CIRCADIAN AVIATION LLC (O2GA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2020-09-15 Matched by certificate designator
ATA 3234

LANDING GEAR WOULD NOT RETRACT WITH GEAR HANDLE SELECTED TO UP POSITION. 3 GREEN ANNUNCIATORS REMAINED ILLUMINATED. DIVERTED BACK TO KMCO. MAINTENANCE REPLACED THE LANDING GEAR HANDLE CONTROL ASSEMBLY. GEAR SWINGS PERFORMED WITH NO DEFECTS NOTED. A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2020091850001 · FAA SDRS
J · 2020-05-28 Matched by certificate designator
ATA 3240

LOW BRAKE PRESS & ANTI-SKID INOPERATIVE ANNUNCIATOR LIGHTS ILLUMINATED & REMAINED ON AFTER SELECTING GEAR DOWN. CREW APPLIED ABNORMAL CHECKLIST AND DIVERTED TO KMIA FOR RUNWAY LENGTH. EMERGENCY WAS DECLARED. LANDING WAS UNEVENTFUL. MAINTENANCE REPLACED THE BRAKE CONTROL MOTOR RELAY, ANTI-SKID PRESSURE SWITCH, BRAKE HYDRAULIC PUMP, AND BRAKE PUMP MOTOR. GEAR SWINGS AND OPS CHECKS WERE GOOD. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2020060450001 · FAA SDRS
O · 2018-06-07 Matched by certificate designator
ATA 5210

A LOUD POP SOUND FROM MAIN ENTRY DOOR FOLLOWED BY CONTINUOUS SOUND OF AIR LEAKING PAST DOOR. CABIN REMAINED PRESSURE. DIVERTED. MAINTENANCE REPLACED MAIN ENTRY DOOR LOWER ACOUSTIC SEALS. OPS CHECKED OK. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2018061150001 · FAA SDRS
O · 2016-07-12 Matched by certificate designator
ATA 7797

LEFT ENGINE ITT GUAGE INOPERATIVE IN FLIGHT. MAINTENANCE REPLACED DEFECTIVE ENGINE T1 HARNESS. ENGINE RUNS PERFORMED AND OPERATIONAL CHECKS WERE GOOD. A SUCCESSFUL OPERATIONAL CHECK WAS ALSO PERFORMED. AIRCRAFT WAS RTS.

Source: SDR O2GA2016071850001 · FAA SDRS
B · 2016-03-03 Matched by certificate designator
ATA 3160

APPROXIMATELY 1.5 HOURS INTO FLIGHT THE MULTI-FUNCTION DISPLAY WENT BLANK, FOLLOWED BY ELEC SMELL. CREW DONNED THEIR OXYGEN MASKS & DIVERTED. LANDING WAS UNEVENTFUL. REPLACED THE MULTI-FUNCTION DISPLAY. SYS OPERATIONAL CHECKS WERE PERFORMED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2016030350001 · FAA SDRS
N · 2015-10-25 Matched by certificate designator
ATA 3260

ON APPROACH, GEAR WAS SELECTED DOWN, RESULTING IN NO LEFT GREEN MAIN UNLOCK LIGHT FOLLOWED BY RED GEAR UNLOCK LIGHT. QUICK DECISION WAS MADE TO CYCLE THE GEAR HANDLE RESULTING IN 3 GREEN GEAR DOWN & LOCKED ANNUNCIATOR LIGHTS. LANDING WAS UNEVENTFUL. ACFT WAS FERRIED WITH GEAR EXTENDED TO MFG SERVICE CTR TO PERFORM GEAR EXTENSION & RETRACTION. TROUBLE SHOT THE DISCREPANCY TO A FAULTY LT GEAR ACTUATOR DOWN LOCK SWITCH. THE LT MLG ACTUATOR WAS REPLACED, GEAR SWINGS PERFORMED WITH NO DEFECTS NOTED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2015102550001 · FAA SDRS
B · 2015-09-11 Matched by certificate designator
ATA 3160

DURING CRUISE AT FL400, PILOTS PFD WENT BLANK & CHECK PFD 1 ANNUNCIATOR ILLUMINATED, FOLLOWED BY A STRONG ELEC BURNING SMELL. CREW FOLLOWED CHECKLIST FOR FIRE & SMOKE, DECLARED AN EMER & DIVERTED. LANDING WAS UNEVENTFUL. ACFT WAS MET BY FIRE RESCUE PERSONNEL. TROUBLE SHOT THE DISCREPANCY TO A FAULT PILOT PFD. THE DISPLAY UNIT WAS REPLACED WITH NO DEFECTS NOTED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2015091450001 · FAA SDRS