N505QS
Operators of this aircraft
Who operated this tail, and how firmly we know it.
| Operator | Role | Period | Basis |
|---|---|---|---|
| NETJETS AVIATION, INC. (DXTA) | Certificate holder | — | Matched by certificate designator |
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
EMER LIGHTS DO NOT COME ON IN THE ARM POSITION ON PREFLIGHT. REMOVED NR 1 EMERGENCY LIGHT POWER SUPPLY AND INSTALLED A NEW #1 OUTRIGHT EMERGENCY LIGHT POWER SUPPLY IAW MM 33-50-06. OPS TEST IS GOOD AND NO DEFECTS NOTED.
INTERIOR REAR EMERGENCY LIGHT ON LAV BULKHEAD & EXIT LIGHT BELOW LAV SEAT INOP WHEN USING BATTERY PACK. BOTH FUNCTION ON SHIPS MAIN BATTERY POWER. POSITIONED THE ACFT INSIDE HANGAR. APPLIED POWER & ALLOWED ACFT TO BOOT UP & VERIFIED THE WRITE-UP. REMOVED THE BATTERY PACK NR 4 DUE TO INTERNAL FAILURE. INSTALLED A NEW BATTERY PACK. PERFORMED OPS CHECK, & THE RESULT WAS SATISFACTORY. ALLOWED BATTERY TO CHARGE WHILE THE GPU WAS IN USE. RETURNED ACFT TO ITS ORIGINAL CONFIGURATION. DONE IAW AMM 33-50-06.
EMERGENCY FLOOR LIGHT BELOW LAV SEAT INOPERATIVE. REMOVED AND REPLACED LAV SEAT TOEKICK LIGHT ASSEMBLY IAW SPM 20-30-0A PERFORMED OPS CHECK OF THE EMERGENCY LIGHTS YAW IAW AMM 33-50-00, OPS CHECKED GOOD.
ON PREFLIGHT EMER LIGHTS WERE ARMED AND FAILED TO ILLUMINATE. PER MCC PROCEDURE, THE APU WAS STARTED AND GIVEN 30MIN TO CHARGE. THEN, THE AIRCRAFT POWERED DOWN AND EMER LIGHT FAILED TO ILLUMINATE AGAIN. REMOVED AND REPLACED EMERGENCY BATTERY PACKS 1,2,3 AND 4. OPS CHECKS OF BATTERIES AND EMERGENCY LIGHTING GOOD AT THIS TIME. TOOK PHOTOS AS RECORD. NO OTHER DEFECTS NOTED. REF. CE680A MM 33-50-06.
LAV OVERHEAD LIGHT. LAV EMER LIGHT UNDER TOILET. LAV FLOOR LIGHT. AND REAR BULKHEAD EXIT SIGN ARE ALL INOP IN ARM MODE. IN ON MODE ALL EMER LIGHTS ARE INOP. TRIED TO CHARGE SYSTEM PER NOTE WITH LIGHT SWITCH IN OFF POSITION FOR 30 MINUTES WITH NO CHANGES. REMOVED FAULTY #4 EMERGENCY BATTERY P/N CBS28-1 S/N 5663M AND INSTALLED CUSTOMER SUPPLIED REPAIRED EMERGENCY BATTERY P/N CBS28-1 S/N 4152M. OPS CHECKS GOOD. WORK DONE !AW CE-680A AMM 33-50-06.
UPON 1ST FLIGHT CHECKS, FOUND MULTIPLE CABIN (+ 1 EXTERIOR) EMERGENCY LIGHTS INOP: EXIT SIGNS: BULKHEAD ABOVE SEAT 7, ABOVE LAV SEAT & BELOW LAV SEAT; PATH LIGHTING: BELOW SEATS 5, 8 & LAV; OVERHEAD SEAT LIGHT: LAV; EXTERIOR OVERWING LIGHT (OVER RIGHT WING). NOTE: WITHOUT DC POWER APPLIED NO EMER LIGHTS COME IN WITH EMER SWITCH IN THE ON POSITION. TROUBLESHOT SYSTEM AND FOUND NO DEFECTS AT THIS TIME, EMERGENCY LIGHT WERE SATISFACTORY IAW MM 33-00-00
NLG LANDING GEAR RETRACTION: ON APPROACH, AFTER GEAR HAD BEEN EXTENDED FOR A WHILE AND FLAPS HAD BEEN SELECTED TO FULL, WE GOT THE AMBER WOW MISCOMPARE CAS. WE INITIATED A MISSED APPROACH, DURING WHICH WE BROUGHT THE GEAR HANDLE UP, BUT GEAR WOULD NOT RETRACT. WE DIVERTED TO A LONGER RUNWAY; GEAR EXTENSION AND LANDING WERE NORMAL. AT SOME POINT DURING TAXI THE WOW MISCOMPARE CAS EXTINGUISHED. // SIGNOFF// REMOVED NLG WIRE HARNESS AND INSTALLED A NEW CUSTOMER SUPPLIED NLG WIRE IAW CE680A AMM 32-20-00. PERFORMED OPERATIONAL CHECK OF MLG EXTENSION AND RETRACTION IN REFERENCE TO CE-680A AMM 32-30-00. OPS CHECK GOOD AT THIS TIME. PN ON: 8469800-2 PN OFF: 8469800-1
MAIN DOOR: CABIN DOOR INTERMITTENTLY CLOSES HALF WAY THEN STOPS AND FALLS OPEN WITH EXTERIOR AMBER CHECK DOOR HANDLE LIGHT ILLUMINATED. TURNING DOOR SWITCH OFF, AMBER LIGHT EXTINGUISHES AND DOOR CLOSES NORMALLY. OPS CHECKED THE DOOR MULTIPLE TIMES AND WE WERE UNABLE TO DUPLICATE THE DISCREPANCY. CALLED MCC NO PREVIOUS HISTORY ON THIS ITEM, WORK IAW AMM 52-00-00. OPS CHECK GOOD, OK TO CONTINUE.
FOUND CORROSION AT LH HORIZONTAL UPPER SKIN AT TIP CAP. COMPLIED WITH TEXTRON AVIATION ENGINEERING ORDER, DQ35708M1, 680A-0042 (N505QS) HORIZONTAL STABILIZER (LEFT UPPER) SKIN DAMAGE (CORROSION).
R/H INBOARD FLAP HAS A GOUGE ON THE UPPER SURFACE APPROXIMATELY 14" FROM OUTBOARD EDGE AND 1" FROM TRAILING EDGE, MEASURING .5" IN LENGTH AND .03 IN WIDTH, FROM A TOOL FALLING ON THE FLAP. ACCOMPLISHED TEXTRON AVIATION ENGINEERING ORDER, DQ35433M1, DATED: JULY 5, 2022. RIGHT WING INBOARD FLAP UPPER SKIN GOUGE REPAIR.
NDI REQUIRED ON FUSELAGE SKIN SCRATCH BEHIND RH FORWARD OVER WING FUSELAGE FAIRING SPLICE STRAP AT FS 354. COMPLIED WITH TEXTRON AVIATION ENGINEERING ORDER, DQ35681M1, FUSELAGE (RIGHT SIDE) DAMAGE (SCRATCH), DATED: JULY 28, 2022.
R/H INBOARD FLAP HAS A GOUGE ON THE UPPER SURFACE APPROXIMATELY 14" FROM OUTBOARD EDGE AND 1" FROM TRAILING EDGE, MEASURING .5" IN LENGTH AND .03 IN WIDTH, FROM A TOOL FALLING ON THE FLAP.
MAIN DOOR: UPON ARRIVAL AND WHILE DEPARTING THE AIRCRAFT, THE MAIN CABIN DOOR WOULD NOT SELF-RELEASE WHEN DOOR HANDLE WAS SELECTED TO THE OPEN POSITION. REPEAT WRITE UP. COMPLETED 3 OPERATIONAL CHECKS OF MAIN CABIN DOOR. FOUND TO BE ACCEPATABLE IN OPERATION WITH A SLIGHT NUDGE. NOTIFED MCC. MCC RECOMMENDED THE DOOR GAS STRUT RIGGING CHECKED. GAINED ACCESS TO GAS STRUT. FOUND THE STRUT RIGGING TO BE NOT IN A NEUTRAL POSITION PER AMM. ADJUSTED GAS STRUT TO PROPER RIGGING. C/W S DOOR OPERATIONAL CHECKS AND DOOR NOW FREE FALLS ON ITS OWN FROM CLOSED POSTION AS REQUIRED. ALL WORK PER CE680A AMM 52-10-00. CLOSE UP ACCESS AS NEEDED.
MAIN DOOR: NOTICED THAT WHEN OPENING THE MAIN CABIN DOOR, THE DOOR DOES NOT FREE-FALL OPEN REGULARLY ESPECIALLY FROM THE OUTSIDE. IT WILL POP THE SEAL BUT STAY IN THE SLIGHTLY AJAR POSITION. FOUND DOOR SUPPORT STRUT TO HAVE A STICKY SUBSTANCE ON IT. CLEANED SUPPORT STRUT OPS CHECKS OF THE DOOR IS GOOD AT THIS TIME ALL WORK DONE IAW CESSNA 680A AMM CHAPTER S2-10-40
LAV EMERG LIGHT: LAV EMERGENCY LIGHT BELOW TOILET INOP. FOUND THE MOLEX CONNECTOR FOR THE LAV TOE KICK LIGHTING HAD THE WIRES PULLED OUT OF IT. RECONNECTED THE WIRES TO THE MOLEX CONNECTORS AND PERFORMED SATISFACTORY OPS CHECK. WORK PERFORMED IAW CE680A AMM 30-50-00 AND CE680A 20-30-15
MAIN DOOR: MAIN CABIN DOOR DOES NOT OPEN PROPERLY AND REQUIRES EXCESSIVE FORCE TO OPEN. ONCE LATCH IS RELEASED, DOOR OPENS ABOUT 3 INCHES THEN STOPS AND DOOR HAS TO BE PUSHED OR PULLED TO OPEN FULLY. CORRECTIVE ACTION: CONFIRMED DOOR SEAL WAS CAUSING THE MED TO HANG UP. REINSTALLED DOOR SEAL AND MED WAS HANGING UP AGAIN. LOOSENED UPPER CORNERS AND REINSTALLED DOOR SEAL + CLEAN & LUBRICATED DOOR SEAL AND OPENED DOOR SEVERAL TIMES FROM INSIDE AND OUTSIDE OF AIRCRAFT AND NOW DOOR OPENS FULLY NORMALLY WITHOUT EXTRA FORCE NEEDED. OPS CHECK GOOD
NLG WHEEL WELL WEB AND UPPER MID FRAME CRACKED. TEXTRON AVIATION STANDARD REPAIR SR-680A-ATA53-25890 DATED: 6-1-2020, CRACK DAMAGE, NOSE LANDING GEAR WHEEL WELL (NWW) FRAME WEB, AND DOUBLERS FS 75. WITH FAA FORM 8100-9 DATED: 6-1-2020.
REPAIR OF NLG WHEEL WELL WEB AND UPPER MID FRAME CRACKS. TEXTRON AVIATION STANDARD REPAIR SR-680A-ATA53-25890 DATED 6/1/2020, CRACK DAMAGE, NOSE LANDING GEAR WHEEL WELL (NWW) FRAME WEB, AND DOUBLERS FS 75. WITH FAA FORM 8100-9 DATED 6/1/2020.
REPAIR RIGHT-HAND HORIZONTAL TIP CAP DAMAGE (EROSION). TEXTRON AVIATION ENGINEERING REPAIR LETTER DQ25536M1 DATED APRIL 22, 2020.
NLG VIBRATION AFTER RETRACTION, AFTER START AND DURING TAXI NWS OPERATED NORMALLY. TAKEOFF ROLL AND ROTATION ALSO NORMAL. RAISED THE LANDING GEAR AND IMMEDIATELY HAD A VERY PRONOUNCED 2 PER SECOND VERTICAL VIBRATION AND LOUD THUMPING NOISE. IT FELT LIKE THE NOSE GEAR HUNG UP IN THE WHEEL WELL. AFTER 5 SECONDS, EXTENDED THE GEAR AND VIBRATION AND NOISE STOPPED AND DISPLAYED 3 GREEN. RETURNED FOR LANDING WHICH WAS NORMAL. AIRCRAFT TAXIS NORMALLY. NOTICED A WOW MISCOMPARE CAS DURING THE EMERGENCY RETURN. NO DAMAGE FOUND ON POST FLIGHT. FOUND NOSE GEAR STRUT TO BE UNDERSERVICED. SERVICED THE STRUT IAW MM 12-20-15. PERFORMED MULTIPLE GEAR SWINGS ALL OPS CHECKED GOOD.
FIVE SECONDS AFTER ADDING TAKEOFF POWER REAR BAY OVERHEAT LOOKUP LIGHT ILLUMINATED. LIGHT WENT OUT TWO SECONDS AFTER THROTTLE REDUCED TO IDLE. RAN ENGINES. CHECKED FOR LEAKS, NO LEAKS FOUND AT THIS TIME. FOUND HEAT BLANKET NOT SECURE ON EXPANSION PIPE OUTBOARD TEMP CONTROL VALVE. RADIATING HEAT ON OVERHEAT LOOP. SECURED BLANKET. RAN UP FULL POWER 30 SEC 3 TIMES WITH NO OVERHEAT LIGHT IAW HAWKER 1000 M/M 26-13-00.
AT FL370 A BURNING ODOR WAS DETECTED, LASTING ABOUT 3-5 MINUTES. ANOTHER DIFFERENT BURNING ODOR WAS DETECTED PASSING 15,000 FEET IN THE DESCENT, IT LASTED UNTIL THE BLEED AIR WAS TURNED OFF PASSING 10,000 FEET. RAN ENGINES AND CHECKED OIL LEVEL. NR 2 ENGINE WAS .25 INCH FROM THE TOP. NR 1 ENGINE .75 INCH FROM THE TOP. RAN ENGINES AGAIN AT ALL POWER LEVELS AND INDIVIDUALLY ONE AT A TIME FOR AN HOUR. CONSECUTIVELY RAN ALL AVIONICS AND BLEED AIR ITEMS. NO ODOR. SHUT DOWN AND DESERVICED APPROX 1 PINT ENGINE OIL FROM NR 2 ENGINE. RAN AGAIN FOR 30 MINUTES. NO ODOR AT THIS TIME.
ON DESCENT WITH POWER LEVERS AT IDLE NOTICED EXHAUST FUME ODOR IN CABIN. REMOVED COALESOR SOCK AND INSTALLED NEW IAW MFG M/M CHAPTER 21-50-13. RAN AIRCRAFT AND LEAK CHECKED, NO LEAKS NOTED, COULD NOT DUPLICATE SMELL AT IDLE ON GROUND.