N5116

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2008-08-20 Matched by certificate designator
ATA 7532

THE "L-BLEED PRESSURE HIGH" AMBER CAS WAS NOTED ON TAKEOFF ROLL BEGINNING. LT ENG BLEED AIR PRESSURE REGULATING VALVE FAILED TO REGULATE PROPERLY. TROUBLESHOOTING REQUIRED. DEFERRED LT BLEED AIR SYSTEM PER MEL 36-1.1 AND COMPLETED TASK M 36.1.1. ACFT WAS RETURNED TO SERVICE. REMOVED AND REPLACED THE LT ENG BLEED AIR REGULATING AND SHUTOFF VALVE. LEAK CHECK PER CMP CODE 710007 AND OPERATIONAL CHECK PER CMP CODE 361215 "BLEED SYSTEM OPERATIONAL CHECK" WERE GOOD. THE DEFERRAL HAS BEEN CLEARED AND ACFT RETURNED TO SERVICE.

Source: SDR UG8A08GM08181 · FAA SDRS
N · 2004-03-31 Matched by certificate designator
ATA 2611

DURING DESCENT, BAGGAGE SMOKE LIGHT (EICAS) CAME ON. NO SMOKE OR FUMES DETECTED ON INSPECTION AFTER LANDING. BAGGAGE SMOKE DETECTOR FOUND TO BE VERY DIRTY. REMOVED SMOKE DETECTOR AND CLEANED COVER AND MOUNTING AREA. REINSTALLED AND PERFORMED FUNCTIONAL CHECK. SYSTEM CHECKED GOOD. INITIATED A FLEET INSPECTION AND CLEANING OF DETECTORS.

Source: SDR UG82004F00002 · FAA SDRS
N · 2004-03-31 Matched by certificate designator
ATA 2611

BAGGAGE SMOKE LIGHT(EICAS) CAME ON. NO SMOKE OR FUMES DETECTED ON INSPECTION AFT LANDING. BAGGAGE SMOKE DETECTER FOUND TO BE VERY DIRTY. INITATED A FLEET INSPECTION AND CLEANING OF DETECTERS. REMOVED SMOKE DETECTER AND CLEANED ALSO CLEANED COVER AND MOUNTING AREA. REINSTALLED AND PERFORMED FUNCTIONAL CHECK. SYSTEM CHECKED GOOD.

Source: SDR GM0409 · FAA SDRS
J · 2004-02-02 Matched by certificate designator
ATA 2210

BLUE YAW DAMPER, FAIL LOWER 'B' CAS MESSAGE, AMBER YAW DAMPER OFF LOWER CAS MESSAGE AND PRI STAB TRIM FAIL AND MACH TRIM OFF CAS MESSAGE CAME ON DURING FLIGHT. CHANNEL 'B' YAW DAMP ACTUATOR FAILED TO OPERATE. REPLACED CHANNEL 'B' YAW DAMP ACTUATOR. OPERATIONAL CHECK NORMAL. (M)

Source: SDR 2004F00088 · FAA SDRS
B · 2003-06-20 Unresolved
ATA 8000

RIGHT ENGINE REPORTED AS SMOKING BY TOWER AND OTHER AIRCRAFT DURING TAXI OUT. RIGHT ENGIEN STARTER FAILED TO DISENGAGE AFTER START. STARTER WAS REPLACED, SERVICED AND OPERATIONALLY CHECKED. RIGHT ENGINE STARTER CHECK GOOD PER CESSNA CITATION X MM AND THE AIRCRAFT WAS RETURNED TO SERVICE. (M)

Source: SDR 2003F00511 · FAA SDRS
J · 2003-05-20 Matched by certificate designator
ATA 2720

DURING PILOT'S PREFLIGHT, WITH APU RUNNING, THE 'RUDDER LIMIT FAIL' RED CAS MESSAGE ANNUNCIATED. ANOTHER AIRCRAT WAS UTILIZED FOR THE TRIP. THE RUDDER LIMITER FAILED TO ACTUATE DUE TO A FAULT IN THE ELECTRICAL COMPONENTS OF THE SYSTEM. AIRCRAFT WAS DE-POWERED AND RESET. NO FAULTS WERE NOTED WHEN POWERED UP A SECOND TIME. NO ACTIVE FAULTS WERE NOTED IN IMT. AIRCRAFT WAS RELEASED FOR SERVICE. (M)

Source: SDR 2003F00359 · FAA SDRS
O · 2003-03-01 Matched by certificate designator
ATA 5210

MAIN CABIN DOOR IS HARD TO OPEN FROM THE INSIDE. REPLACED AFT CABLE ASSEMBLY, SPRING PIVOT BEARINGS ANDLONG SHAFT. RIGGED THE DOOR PER CESSNA MM. OPERATIONAL CHECK IS GOOD. AIRCRAFT RETURNED TO SERVICE. (M)

Source: SDR 2003F00227 · FAA SDRS
J · 2002-05-16 Matched by certificate designator
ATA 7200

RIGHT ENGINE OIL PRESSURE OUT OF LIMITS, HI/RED 106 PSI AT 80-90 KTS. ENGINE INTERNAL BEARING SEAL AIR LEAKAGE WHICH MAY OCCUR AS ENGINE APPROACHES ITS MIDLIFE INSPECTION. VISUALLY INSPECTED ENGINE OIL FILTER BYPASS BUTTON. PERFORMED TAKEOFF POWER RUN UP. FOUND OIL PRESSURE WITHIN LIMITS.

Source: SDR UG82002F00002 · FAA SDRS
N · 2002-01-23 Matched by certificate designator
ATA 5270

PSP - MAIN CABIN DOOR WARNING LIGHT WOULD NOT EXTINGUISHED WHEN CLOSED. FAULTY DOOR HANDLE PROXIMITY SWITCH. PROBLEM WAS CORRECTED BY REPLACEMENT OF THE SWITCH. OPERATIONAL CHECK OF SYSTEM WAS GOOD IAW 750 MM CHAPTER 52-70-00. (M)

Source: SDR 2002F00984 · FAA SDRS
E J · 2001-10-18 Matched by certificate designator
ATA 2910

VIBRATION FELT ON CABIN FLOOR AS WELL AS HUM. LT HYD (A) SYSTEM FLUCTUATED BETWEEN 2400-3300 PSI. WHEN GEAR WAS SELECTED DOWN LT HYD PRES WAS 2100 AND RT HAD AN OT (AMBER) LIGHT. UPON LANDING THEY GOT A (B) SYSTEM FAIL MESSAGE, BOTH SYSTEM PRESSURES WERE 1800 PSI. HYDRAULIC SYSTEM MALFUNCTION DUE TO FAILED HYDRAULIC POWER TRANSFER UNIT. FAILED UNIT CAUSE CONTAMINATION IN THE LEFT HYDRAULIC SYSTEM WHICH NECESSITATED THE REPLACEMENT OF THE LEFT HYDRAULIC PUMP, ALL (A) SYSTEM FILTERS AND FLUSHING AND BLEEDING OF THE HYDRAULIC SYSTEM. REPLACED THE HYDRAULIC SYSTEM PTU, LEFT ENGINE DRIVEN PUMP AND ALL (A) SYSTEM FILTERS. HYDRAULIC SYSTEM WAS FLUSHED AND BLED PER AIRCRAFT MAINTENANCE MANUAL.

Source: SDR UG82001F00009 · FAA SDRS
E J · 2001-10-05 Matched by certificate designator
ATA 2910

VIBRATION FELT ON CABIN FLOOR AS WELL AS HUM. LEFT HYDRAULIC (A) SYSTEM FLUCTUATED BETWEEN 2400-3300 PSI. WHEN GEAR WAS SELECTED DOWN LEFT HYDRAULIC PRESSURE WAS 2100 AND RIGHT HAD AN OT(AMBER) LIGHT. UPON LANDING THEY GOT A (B) SYSTEM FALL MESSAGE, BOTH SYSTEM PRESSURES WERE 1800 PSI. APPARENT CAUSE: HYDRAULIC SYSTEM MALFUNCTIONED. MAINTENANCE CORRECTION IN PROGRESS.

Source: SDR UG82001F00008 · FAA SDRS
K · 2001-07-27 Matched by certificate designator
ATA 2910

IND - PILOT WALKAROUND PRIOR TO DEPARTURE, TWO HYD PUDDLES UNDER TAIL OF A/C. 'A' HYD SYSTEM INDICATES 25 PERCENT. APPEARS TO BE COMING FROM ELEVATOR. REPLACED O-RING UNDER HYD FITTING (PRESSURE) ON RIGHT INBOARD PCU. (M)

Source: SDR 2001F00330 · FAA SDRS
J · 2001-07-22 Matched by certificate designator
ATA 3260

DTW - NOSE GEAR WOULD NOT RETRACT. ADJUSTED NOSE GEAR SQUAT SWITCH RAMP. (M)

Source: SDR 2001F00336 · FAA SDRS
O · 2001-04-24 Unresolved
ATA 2421

CREW STATED RIGHT HAND WINDSHIELD HEAT INOPERATIVE. TROUBLESHOT TO FAULTY LEFT HAND ALTERNATOR. UPON ALTERNATOR REMOVAL, NOTICED THAT THE COOLING FAN BLADES ON THE ALTERNATOR WERE ALL BROKEN OFF.

Source: SDR 20010511CW013 · FAA SDRS
J · 1997-12-01 Unresolved
ATA 3222

THE AIRCRAFT DEPARTED DTW AND ON CLIMB-OUT, THE LANDING GEAR HANDLE WOULD NOT MOVE TO THE RETRACT POSITION. THE AIRCRAFT RETURNED TO DTW AND MAINTENANCE WAS UNABLE TO DUPLICATE. GALLING WAS DETECTED IN THE CHROME SECTION OF THE STRUT ASSY AND THE UNIT WAS SENT BACK TO WICHITA FOR EVALUATION.

Source: SDR 98ZZZX340 · FAA SDRS