N511JL

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Accident · 1978-09-04 Unresolved
Beech A55 None injuryoperator not yet resolved
Source: NTSB case CHI78DET37
Accident · 1968-07-23 Unresolved
Beech 95-A55 None injuryoperator not yet resolved
Source: NTSB case CHI69F0115
Accident · 1967-12-20 Unresolved
Beech 95-A55 None injuryoperator not yet resolved
Source: NTSB case CHI68F0551

Maintenance disclosures

O · 2023-02-14 Matched by certificate designator
ATA 2131

FLIGHT CREW REPORTED THAT THE CABIN FAILED TO PRESSURIZE AFTER TAKEOFF. THEY REMAINED AT 9000' ALTITUDE AND RETURNED FOR A NORMAL LANDING AT KORL. THE MAINTENANCE PROVIDER TROUBLESHOT AND DETERMINED THAT THE CABIN PRESSURE CONTROLLER AT FAULT. THE PRESSURE CONTROLLER WAS REMOVED AND A OVERHAULED UNIT WAS INSTALLED. OPS CHECKS WERE SATISFACTORY, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2023022034031 · FAA SDRS
J · 2023-01-26 Matched by certificate designator
ATA 2750

THE FLIGHT CREW INDICATED THAT SHORTLY AFTER TAKEOFF OF RECEIVING A FLASHING AMBER “HYDRAULIC PRESSURE” INDICATION, AND AFTER RECYCLING THE FLAPS THEY RETURNED TO AN INDICATION OF 7 DEGREES BUT NOT THE 5 DEGREES THAT WAS SELECTED. THE FLIGHT CREW ELECTED TO DIVERT THE FLIGHT AND LAND FOR MAINTENANCE EVALUATION. THE MAINTENANCE PROVIDER FOUND THE FLAP CONTROL VALVE DEFECTIVE AND REMOVED IT AND INSTALLED AN OVERHAULED UNIT. OPERATIONAL AND LEAK CHECKS WERE SATISFACTORY, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2023020634028 · FAA SDRS