N514NC

CESSNA 402C · 1981 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-10-18 Matched by certificate designator
ATA 5740

DURING MAINTENANCE 3 SPOTS OF CORROSION WERE VISUALLY IDENTIFIED ON THE OUTBOARD LEFT UPPER AFT WING FITTING (OEM PN: 0822550-45). ALL THREE SPOTS ARE LOCATED ON THE LOWER SURFACE OF THE HORIZONTAL FLANGE OF THIS FITTING, AND ARE CONSISTENT WITH OTHER CORROSION DISCREPANCIES VISUALLY IDENTIFIED IN THIS AREA. THE FIRST LOCATION MEASURES APPROX. .250" WIDE AND .750" LONG. THE OTHER TWO LOCATIONS EACH MEASURE APPROX. .125" BY .125". ALL 3 LOCATIONS ARE APPROX. .015 DEEP. THIS FITTING HAS BEEN CHANGED USING NEW PARTS.

Source: SDR HYIA20241018001 · FAA SDRS
O · 2021-05-11 Matched by certificate designator
ATA 5410

DURING INSPECTION A CRACK WAS VISUALLY DISCOVERED ON THE INBOARD END OF THE LOWER CHANNEL OF THE RIGHT HAND CROSSOVER BEAM. THIS CRACK IS IN THE AREA OF THE MOUNTING HOLES FOR THE INBOARD EXHAUST ELBOW CLAMP BRACKET, AND MEASURES APPROXIMATELY 2 INCHES LONG AND IS CONSISTENT WITH OTHERS VISUALLY IDENTIFIED IN THIS AREA. THIS BEAM HAS BEEN REPLACED USING NEW PARTS.

Source: SDR HYIA20210512001 · FAA SDRS
O · 2020-05-06 Matched by certificate designator
ATA 8530

DURING ROUTINE INSPECTION AND REPLACEMENT OF THE RIGHT ENGINE CYLINDER #3 IT WAS DISCOVERED THAT THE CONNECTING ROD BUSHING OF THE #3 CYLINDER WAS FOUND TO BE DAMAGED AND LOOSE. THE CONNECTING ROD AND CYLINDER WILL BE REPLACED.

Source: SDR HYIA20200508001 · FAA SDRS
O · 2019-01-16 Matched by certificate designator
ATA 5410

DURING MAINTENANCE A CRACK WAS DISCOVERED ON THE RIGHT NACELLE INBOARD CROSSOVER BEAM SUPPORT CHANNEL P/N: 5654102-15. AFTER REMOVING THIS CHANNEL IT WAS DISCOVERED THAT THE RIGHT HAND INBOARD BEAM, P/N: 5654109-7 WAS CRACKED UNDERNEATH THE SUPPORT CHANNEL. THIS CRACK MEASURES APPROXIMATELY .890 INCHES LONG AND COULD NOT BE SEEN UNTIL THE -15 CROSSOVER BEAM SUPPORT WAS REMOVED. THIS BEAM WILL BE REMOVED AND REPLACED USING NEW PARTS.

Source: SDR HYIA20190117001 · FAA SDRS
J · 2018-09-24 Matched by certificate designator
ATA 8500

PILOT REPORTED RIGHT ENGINE OIL PRESSURE DROPPED TO 20 PSI IN FLIGHT AND TO ZERO PSI AT IDLE ON THE GROUND. MAINTENANCE INSPECTED AND FOUND METAL PARTICLES AT THE OIL PRESSURE RELIEF VALVE, FURTHER INSPECTION FOUND THE STARTER ADAPTER NEEDLE BEARING DAMAGED. THE ENGINE IS BEING REPLACED.

Source: SDR HYIA20180926001 · FAA SDRS
O · 2017-05-09 Matched by certificate designator
ATA 5700

DURING A ROUTINE INSPECTION, A CRACK WAS LOCATED AT RIB RT WS. 106.79. THE CRACK WAS 1.5 INCHES IN LENGTH, REPLACED THE RIB IAW MM.

Source: SDR HYIA20170821001 · FAA SDRS
O · 2017-01-04 Matched by certificate designator
ATA 5415

DURING A ROUTINE INSPECTION, TWO CRACKS WERE FOUND IN THE RT OUTBOARD NACELLE FITTING. THESE CRACKS WERE FOUND ON THE INBOARD SIDE OF THE FITTING, JUST FORWARD OF THE SPAR STRAP. THEY MEASURED .119 AND .146 IN LENGTH.

Source: SDR HYIA20170828017 · FAA SDRS
O · 2016-09-27 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160913155 · FAA SDRS
O · 2016-09-27 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160913156 · FAA SDRS
O · 2016-09-27 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160913157 · FAA SDRS
H · 2016-02-03 Matched by certificate designator
ATA 2434

PILOT REPORTED LOSING BOTH ALTERNATORS IN FLIGHT AFTER A MODERATE JOLT OF TURBULENCE, RETURNED WHEN THEY COULD ONLY RESET ONE ALTERNATOR BY FOLLOWING THE QRH PROCEDURE OF REPLACING FIELD FUSES. INSPECTED & REPAIRED SHORTED F1 WIRE IN RT NACELLE, AS WELL AS REMOVED & INSTALLED THE RT ALTERNATOR & VOLTAGE REGULATOR. PARALLELED THE SYS. OPERATIONS CHECKED GOOD AT THIS TIME.

Source: SDR HYIA20160205002 · FAA SDRS
N · 2015-02-26 Matched by certificate designator
ATA 5270

PILOT REPORTED CABIN DOOR OPEN ON TAKEOFF. INSP THE MAIN CABIN DOOR TOP & BOTTOM WITH NO DISCREPANCY NOTED. REPLACED WORN SPRING ON THE OUTSIDE HANDLE AS PRECAUTION. OPERATIONAL CHECKED OK.

Source: SDR HYIA20150227002 · FAA SDRS
K B · 2012-05-28 Matched by certificate designator
ATA 2840

PILOT REPORTED A PREVELENT FUEL ODOR DURING ALL GROUND OPERATIONS AND DURING CLIMBOUT. PILOT NOTED WHAT APPEARED TO BE FUEL IN BOTTOM OF FUEL FLOW INDICATOR. ON INSPECTION, EVIDENCE OF FUEL STAINS AT THE BOTTOM OF FUEL FLOW GAUGE WERE NOTED. BASED ON THIS FINDING, FUEL FLOW GAUGE WAS R & R IAW C402 MM.

Source: SDR HYIA20120528528 · FAA SDRS
K B · 2012-05-11 Matched by certificate designator
ATA 2140

PILOT REPORTED A FUEL ODOR IN THE COCKPIT. ODOR WAS FOUND TO BE CAUSED BY A LEAKING B-NUT ON THE HEATER FUEL PUMP. B-NUT WAS THEN SECURED, AND THE AREA WAS CHECKED WITH NO LEAKS.

Source: SDR HYIA5112FUELODOR · FAA SDRS
O · 2011-04-15 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE OF MEB91-11R1. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414005 · FAA SDRS
O · 2011-03-11 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE OEM PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415032 · FAA SDRS
K J · 2010-01-24 Matched by certificate designator
ATA 3233

CREW REPORTED, ON APPROACH, AFTER GEAR EXTENSION, GEAR UNLOCK LIGHT REMAINED ILLUMINATED WITH NO RT MLG DOWNLOCK INDICATION. PERFORMED EMERGENCY EXTENSION OF LANDING GEAR, AND DECLARED AN EMERGENCY. LANDING WAS UNEVENTFUL. MX FOUND RT MAIN GEAR DOWNLOCK SWITCH LEAKING AT ACTUATOR. REMOVED AND REPLACED AFFECTED SWITCH SEALS. REPLACED SEAL RETAINER AS A PRECUATIONARY MEASURE. PERFORMED GEAR RETRACTION AND EXTENSIONS CHECKS. NO DEFECTS NOTED. RETURNED ACFT TO SERVICE.

Source: SDR HYIA514NC RMLG · FAA SDRS
B · 2007-06-10 Matched by certificate designator
ATA 2497

CREW SMELLED BURNING ODOR IN COCKPIT DURING FLIGHT. MX INSPECTED AND FOUND WIRES IN NLG WHEEL WELL CHAFED. MX REPAIRED WIRING AND RELEASED A/C.

Source: SDR N514NC · FAA SDRS
H · 2006-04-24 Matched by certificate designator
ATA 2460

CREW REPORTED AVIONICS MASTER SWITCH INOP. MX CHANGED CIRCUIT BREAKER SWITCH, MFG DATE CODE 0527.

Source: SDR 1350527514 · FAA SDRS
O · 2003-05-27 Matched by certificate designator
ATA 3197

AVIONICS MASTER SWITCH INOPERATIVE. MAINTENANCE REPLACED SWITCH AND RETURNED THE AIRCRAFT TO SERVICE.

Source: SDR HYI2003F00008 · FAA SDRS
J · 2001-02-22 Matched by certificate designator
ATA 3222

UPON GEAR RETRACT, HYDR PRES LIGHT REMAINED ILLUMINATED. GEAR EXTENSION WAS ATTEMPTED, NOSE GEAR FAILED TO EXTEND. GEAR WAS EXTENDED USING EMERGENCY BLOW DOWN PROCEDURE, ALL GEAR DOWN INDICATORS SHOWED GREEN AND AIRCRAFT LANDED WITHOUT INCIDENT. MECH FOUND NOSE GEAR STRUT FLAT AND ALL FOUR NOSE GEAR DOOR ATTACH BRACKETS BROKEN. WHEN THE GEAR WAS RETRACTED, COMPRESSED NOSE STRUT FAILED TO ENTER WHEEL WELL PROPERLY, DAMAGING THE GEAR DOOR BRACKETS AND CAUSED THE GEAR TO STICK IN THE WELL. THE STRUT WAS SERVICED, BRACKETS REPLACED. EXTENSION AND RETRACTION TEST WAS PERFORMED, ALL INDICATIONS NORMAL. AC RETURNED TO SERVICE.

Source: SDR 20010403CW011 · FAA SDRS