N522AC

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
SCOTT AVIATION, LLC (K95A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

E · 2020-12-30 Matched by certificate designator
ATA 7200

SHORTLY AFTER OUR INITIAL DESCENT FROM CRUISE ALTITUDE, DESCENDING THROUGH ABOUT 37,000 FEET, WE EXPERIENCED A LOUD, HIGH FREQUENCY VIBRATION. WHILE ADJUSTING THRUST IN ORDER TO DETERMINE THE CAUSE OF THE VIBRATION, WE NOTICED INCREASING ITT ON THE RIGHT ENGINE. PASSENGERS WERE INFORMED WE WERE DEALING WITH A MECHANICAL ISSUE AND INSTRUCTED TO RETURN TO THEIR SEATS, (LEAD PAX WAS IN THE GALLEY), SECURE THEIR SEATBELTS AND REMAIN THERE. RT ENGINE VIB MESSAGE ILLUMINATED AS WE WERE ALREADY WORKING THROUGH THE ENGINE VIBRATION CHECKLIST, AND ITT STABILIZED WITH THE RIGHT ENGINE AT IDLE, BUT REMAINED ABNORMALLY HIGH. HIGH FREQUENCY VIBRATION CONTINUED. WE ELECTED TO SHUTDOWN THE RIGHT ENGINE, DECLARED AN EMERGENCY, AND WERE GIVEN DIRECT DESTINATION (KAPA). VIBRATION INSTANTLY STOPPED WITH THE RIGHT ENGINE SECURED. WHILE CONTINUING TO DESCEND TOWARD OUR DESTINATION AND WORKING THROUGH THE ENGINE SHUTDOWN INFLIGHT CHECKLIST, THE VIBRATION RESUMED. UNCERTAIN OF WHAT WAS CAUSING THE VIBRATION WITH THE DAMAGED ENGINE SECURED, WE ELECTED TO DIVERT TO THE NEAREST SUITABLE AIRPORT INSTEAD OF CONTINUING ON TO OUR ORIGINAL DESTINATION. UPON INSPECTION OF THE ENGINE, FOUND THE NUMBER 4 BEARING SEIZED WHICH DAMAGED THE HP SHAFT ALONG WITH THE MAJORITY OF THE AFT ROTATING COMPONENTS.

Source: SDR AMCR20210108 · FAA SDRS
W · 2010-08-26 Matched by certificate designator
ATA 3530

FOUND PORTABLE O2 MASK TO BE THE INCORRECT TYPE. EVEN THOUGH CUSTOMER BULLETIN 213 DID NOT LIST THIS ACFT IN THE EFFECTIVITY SECTION, AN INSP REVEALED THE WRONG MASK ANYWAY. ANOTHER BAD MASK WAS FOUND ON ANOTHER ACFT IN THE FLEET ALSO NOT LISTED IN THE BULLETIN. RECOMMEND ALL THESE OPERATORS CHECK THEIR PORTABLE O2 MASK FOR CORRECT PN IAW CB213.

Source: SDR AMCR201008 · FAA SDRS
O · 2010-05-26 Matched by certificate designator
ATA 3244

(AMCR) DURING POSTFLIGHT INSPECTION, MX FOUND A BULGE ON THE LT NOSE TIRE. THE BULGE WAS ABOUT 1 INCH DIAMETER AND EXTENDED OUT .2500 INCH. THE BULGE WAS LOCATED ON THE SIDEWALL JUST BELOW THE TREAD CAP.

Source: SDR AMCR201002 · FAA SDRS
J · 2005-11-29 Matched by certificate designator
ATA 5230

CREW NOTED A WHISTLE FROM BAGGAGE DOOR AREA. MAINTENANCE FOUND THE BAGGAGE DOOR SEAL TORN IN THE 12 O'CLOCK POSITION. IT APPEARS THAT THE TOP BAYONET LATCH PLATE ON THE FUSELAGE HAD EXCESS SEALANT ON THE IB SIDE, CAUSING THE DOOR SEAL TO RUB HARD AGAINST IT DURING DOOR CLOSING. DOOR SEAL REPLACED AND EXCESS SEALANT REMOVED FROM BAYONET PLATE. OTHER AIRCRAFT IN FLEET WERE INSPECTED AND NO EXCESS SEALANT WAS FOUND ON THOSE PLATES.

Source: SDR AMCR200500010 · FAA SDRS
F · 2005-09-15 Unresolved
ATA 2210

DURING CLIMB, CREW COULD NOT ENGAGE AUTOPILOT. DURING HAND FLYING, CREW GOT SEVERAL UNCOMMANDED GO-AROUND COMMANDS IN WHICH COMMAND BARS WOULD POP-UP AND THROTTLES WOULD ADVANCE TO FULL POWER. MX FOUND THE BODY OF GO-AROUND SWITCH HAD SEPARATED WHICH CAUSED SWITCH TO RECESS A BIT INTO THE YOKE. BECAUSE SWITCH POSTS DID NOT HAVE HEAT SHRINK ON THEM, THEY WERE SHORTING OUT CAUSING THE UNCOMMANDED GO-AROUND SCENERIO. MX ENSURED SHRINK TUBE WAS INSTALLED ON NEW SWITCH.

Source: SDR AMCR200500008 · FAA SDRS
K · 2003-10-30 Unresolved
ATA 2622

DURING BASIC INSPECTION, TECHNICIAN FOUND THE COCKPIT FIRE EXTINGUISHER PRESSURE GAUGE TO BE READING AT VERY BOTTOM OF GREEN RANGE. FURTHER INSPECTION REVEALED THE GAUGE TO BE LOOSE, AND SLIGHTLY TWISTING GAUGE CAUSED THE BOTTLE TO LEAK.

Source: SDR AMCR200300007 · FAA SDRS