N544LM

GATES LEARJET CORP. 35A · 1983 · Valid Registration

Registered owner: CORSAIR TWO LLC, OR (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AERO AIR LLC (O9IA)Certificate holderMatched by certificate designator
AERO AIR LLC (O9IA)Operator2012-03-05 – 2012-03-05Operator named in NTSB report

Accident & incident history

Inc · 2012-03-05 Operator named in NTSB report
BOMBARDIER LEARJET CORP. 35A None injury Part 135AERO AIR LLC
Source: NTSB case ANC12IA024

Maintenance disclosures

J · 2018-04-29 Matched by certificate designator
ATA 3230

DURING APPROACH, CREW SELECTED GEAR DOWN. ONLY RECEIVED THE GREEN LIGHT ON THE NOSE GEAR AND HAD RED LIGHTS ON THE MAIN GEAR. GEAR WAS CYCLED UP AND ALL LIGHTS WENT OUT AS NORMAL. SECOND ATTEMPT TO LOWER GEAR RESULTED IN NO LIGHTS. TRIED TWO MORE TIMES WITH THE SAME RESULTS. CREW ALERTED THE TOWER AND ABORTED THE LANDING. THE EMERGENCY GEAR EXTENSION WAS THEN USED TO LOWER THE GEAR. ON THE ATTEMPT TO LOWER THE GEAR WITH THE EMERGENCY EXTENSION, AGAIN ONLY THE NOSE GEAR GREEN LIGHT ILLUMINATED AND BOTH MAIN GEAR HAD RED. THEN PERFORMED A FLY BY OF THE TOWER TO CONFIRM GEAR STATUS. TOWER REPORTED THE NOSE LOOKED DOWN, MAIN GEAR DOORS LOOKED OPEN, AND ONLY THE RT GEAR LOOKED LIKE IT WAS PARTIALLY OUT. THE CREW DECLARED THAT THEY WOULD BE LANDING WITH THE GEAR UP. WHEN IN THE PATTERN TO LAND, THE CREW TRIED ONE MORE TIME TO EXTEND THE GEAR UTILIZING THE EMERGENCY EXTENSION SYSTEM AND GOT ALL THREE GREEN LIGHTS. AIRCRAFT LANDED SAFELY. OPEN

Source: SDR O9IA2018042900001 · FAA SDRS
N · 2018-03-07 Matched by certificate designator
ATA 2612

DURING CRUISE, THE RT ENGINE FIRE LIGHT ON THE T HANDLE CAME ON IN FLIGHT. NO OTHER ABNORMAL INDICATIONS WERE NOTED. POWER WAS RETARDED AND LIGHT EXTINGUISHED RIGHT AWAY. POWER WAS BROUGHT BACK UP AND NO ABNORMALITIES THE REMAINING PORTION OF THE FLIGHT. AIRCRAFT LANDED WITHOUT INCIDENT. MAINT INSPECTED THE ENGINE COMPARTMENT FOR DAMAGE AND NOTED NONE. INSPECTION OF THE FIRE LOOP SYSTEM ALSO PRODUCED NO FAULTS. AIRCRAFT WAS RUN UP TO CHECK SYSTEM UNDER POWER WITH NO ISSUES. PERFORMED A MAINT CHECK FLIGHT AND NO ISSUES WERE NOTED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O9IAN544LM030718 · FAA SDRS
B · 2018-01-24 Matched by certificate designator
ATA 2121

STRONG ELECTRICAL BURNING ODOR IN CABIN, DURING CLIMB. FOUND THE VENT BLOWER MOTOR SEIZED. REMOVED THE BLOWER MOTOR AND FOUND IT WAS NOT ROTATING SMOOTHLY. REPLACED THE UNIT WITH AN OVERHAUL UNIT. OPERATIONAL CHECKED GOOD.

Source: SDR O9IAN544LM012418 · FAA SDRS
W B · 2013-10-08 Matched by certificate designator
ATA 5100

SMOKE SEEN COMING FROM IN FRONT OF DIVAN SEAT. INVESTIGATION REVEALED POOR INSULATION COVERING THE LT WING/STAB HEAT DUCT PIPE. THIS PIPE WAS REWRAPPED WITH INSULATION MATERIAL. RESULTANT CHECK FLIGHT WAS SATISFACTORY.

Source: SDR O9IA20131008544 · FAA SDRS
B · 2013-10-06 Matched by certificate designator
ATA 3010

WHEN WING AND STAB HEAT TURNED ON, THERE IS A BURNING ODOR IN CABIN AND COCKPIT. GROUND RUNS/CHECKS WERE UNABLE TO IDENTIFY PROBLEM. CHECK FLIGHT PERFORMED. NO FINDINGS. SECOND IDENTIFIED VERY LIGHT SMOKE FROM LT WING/STAB HEAT PIPE. PIPE HAD BEEN REWRAPPED WITH INSULATION AND A HEAT TAPE UTILIZED TO KEEP IN PLACE. TAPE ADHESIVE WAS GETTING HOT AND EMITTING SMOKE AND FUMES. REWRAPPED DUCT WITHOUT TAPE. SUBSEQUENT FLIGHT CHECKS REVEALED NO DISCREPANCY.

Source: SDR O9IA544LM100613 · FAA SDRS
B · 2013-05-17 Matched by certificate designator
ATA 3010

PASSENGERS COMPLAINED OF BURNING PLASTIC ODOR WHICH MADE THEM NAUSEAS. FOUND WING ANTI-ICE DUCT HEAT SHIELD OUT OF POSITION ALLOWING HEAT TO BE TRANSFERRED TO PLASTIC. ADJUSTED AND PERFORMED SYS CHECK WITH NO DISCREPANCIES FOUND. A SUBSEQUENT FLIGHT HAD A BURNING PLASTIC ODOR AND WHEN A FLIGHT CREW MEMBER STEPPED BACK TO INVESTIGATE A SLIGHT VISUAL AMOUNT OF SMOKE WAS SEEN IN AREA OF WING DE-ICE DUCT. SUBSEQUENT INSPECTION REVEALED THAT THE INSULATION BLANKET HOOK AND LOOP STRIP HAD COME IN CONTACT WITH BARE METAL OF DE-ICE DUCT. COVERED DE-ICE DUCT WITH HEAT SHIELD. NO FURTHER FAULTS FOUND.

Source: SDR O9IA2013052000001 · FAA SDRS
F · 2012-06-13 Matched by certificate designator
ATA 3297

DURING APPROACH, FLIGHT CREW SELECTED GEAR DOWN. GEAR DID NOT EXTEND. SECOND ATTEMPT WAS TRIED WITH SAME RESULTS. LANDING GEAR WAS EXTENDED USING EMERGENCY EXTENSION PROCEDURES. LANDING . INVESTIGATION REVEALED FAULTY CONNECTOR ON LANDING GEAR SELECTOR VALVE. CONNECTOR REPLACED, LANDING GEAR LINES PURGED, HYD SERVICED AND BLED. GEAR SWINGS PERFORMED WITH NORMAL RESULTS.

Source: SDR O9IA2012F00126 · FAA SDRS
B · 2011-06-25 Matched by certificate designator
ATA 2121

ON DESCENT, THE FLIGHT CREW SMELLED AN ELECTRICAL BURNING ODOR IN THE CABIN. CREW DECLARED AN EMERGENCY AND LANDED WITHOUT INCIDENT. DURING THE APPROACH CREW HAD DEPLOYED OXYGEN MASKS FOR NURSES/PATIENT ON BOARD ACFT. INVESTIGATION OF ACFT FOUND NO HOT SPOTS. IDENTIFIED CABIN BLOWER FAN AS FAILING. REMOVED FROM ACFT.

Source: SDR O9IA003Y 6.25.11 · FAA SDRS