N555LK

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

F · 2023-05-14 Matched by certificate designator
ATA 2780

WHILE CONDUCTING A PART 135 FLIGHT THE CREW OF N555LK OBSERVED A NO FLAP MOVEMENT SITUATION WHEN COMMANDED TO LANDING CONFIGURATION ON APPROACH INTO KPBI AND DECLARED AN EMERGENCY IN RESPONSE TO THE LACK OF FLAP MOVEMENT. AIRCRAFT LANDED WITHOUT ANY FURTHER ISSUES.

Source: SDR 6TXA202305150001 · FAA SDRS
F · 2023-05-14 Unresolved
ATA 2780

WHILE CONDUCTING A PART 135 FLIGHT THE CREW OF N555LK OBSERVED A NO FLAP MOVEMENT SITUATION WHEN COMMANDED TO LANDING CONFIGURATION ON APPROACH INTO KPBI AND DECLARED AN EMERGENCY IN RESPONSE TO THE LACK OF FLAP MOVEMENT. AIRCRAFT LANDED WITHOUT ANY FURTHER ISSUES.

Source: SDR 2023FA0000281 · FAA SDRS
O · 2022-10-29 Matched by certificate designator
ATA 2130

AIRCRAFT DEPARTED FROM KAPF ON A REPOSITION LEG AT 1300 ENROUTE TO KTMB. LANDED AND PICKED UP 3 PASSENGERS. DEPARTED KTMB FOR KVNY AT 1430. AFTER TAKEOFF DURING CLIMB OUT, OUTFLOW VALVE FULLY CLOSED AND CABIN PRESSURIZED TO -3500 FT. DIFFERENCE OF PRESSURE EXCEEDED 9.9, AND A DECISION WAS MADE TO DIVERT TO KMIA. EMERGENCY OUTFLOW VALVE WAS OPERATED TO RELIEVE PRESSURE AND AIRCRAFT LANDED WITH NO ISSUES AT -2000 FT. ONCE ON THE GROUND, NORMAL OUTFLOW VALVE WAS MANUALLY DRIVEN OPEN TO EQUALIZE PRESSURE. TROUBLESHOOTING COMMENCED, STILL UNKNOWN WHAT THE ISSUE IS AT THIS POINT. WORKING WITH ENGINEERING TO DETERMINE NEXT PHASE OF ACTION BEFORE RTS.

Source: SDR 6TXA 202210298001 · FAA SDRS
O · 2022-10-28 Unresolved
ATA 2130

AIRCRAFT DEPARTED FROM KAPF ON A REPOSITION LEG AT 1300 ENROUTE TO KTMB. LANDED AND PICKED UP 3 PASSENGERS. DEPARTED KTMB FOR KVNY AT 1430. AFTER TAKEOFF DURING CLIMB OUT, OUTFLOW VALVE FULLY CLOSED AND CABIN PRESSURIZED TO -3500 FT. DIFFERENCE OF PRESSURE EXCEEDED 9.9, AND A DECISION WAS MADE TO DIVERT TO KMIA. EMERGENCY OUTFLOW VALVE WAS OPERATED TO RELIEVE PRESSURE AND AIRCRAFT LANDED WITH NO ISSUES AT -2000 FT. ONCE ON THE GROUND, NORMAL OUTFLOW VALVE WAS MANUALLY DRIVEN OPEN TO EQUALIZE PRESSURE. TROUBLESHOOTING COMMENCED AND STILL UNKNOWN WHAT THE ISSUE IS AT THIS POINT. WORKING WITH ENGINEERING TO DETERMINE NEXT PHASE OF ACTION BEFORE RTS.

Source: SDR 2022F00435 · FAA SDRS