N560HD
Operators of this aircraft
Who operated this tail, and how firmly we know it.
No operator established for this aircraft.
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
AIRCRAFT WAS ON APPROACH. CREW EXTENDED LANDING GEAR AND DID NOT GET A NOSE GEAR DOWN AND LOCKED LIGHT. CYCLED GEAR AND ATTEMPTED TO EXTEND THE LANDING GEAR. THE RESULT WAS THE SAME. ALSO NOTED THAT THEY DID NOT HAVE A RED GEAR IN TRANSIT LIGHT. AS THE CREW RAN THE EMERGENCY CHECKLIST, CYCLED THE GEAR CONTROL CIRCUIT BREAKER. AFTER CYCLING THE CIRCUIT BREAKER THE NOSE LANDING GEAR DOWN AND LOCKED LIGHT ILLUMINATED. AIRCRAFT LANDED WITH NO FURTHER ISSUES. INSPECTION RESULTED IN FINDING THE DOWN LOCK SWITCH ON THE NLG ACTUATOR STICKING. ACTUATOR ALSO HAD EXCESSIVE PLAY. ACTUATOR AND SWITCH WERE REPLACED.
AIRCRAFT TOOK OFF FROM KASE. AT 400 AGL THE DOOR SEAL LIGHT ILLUMINATED. AIRCRAFT CONTINUED DEPARTURE ROUTE, SHORTLY AFTERWARDS THE CABIN DOOR LIGHT ILLUMINATED. ATC DIRECTED THE AIRCRAFT ALONG DEPARTURE PATH TO LINDZ INT. CLIMBING TO 12,000 FT. PILOT HEARD A LOUD HISS FROM CABIN DOOR AREA. CABIN ALT. 10000 LIGHT ILLUMINATED. ATC CLEARED AIRCRAFT TO FL 190. CREW PERFORMED EMERGENCY CHECKLIST AND DONNED O2 MASKS. CREW REQUESTED AND RECEIVED DIRECT DESTINATION INTO KAPA. FLIGHT CONTINUED TO KAPA UNEVENTFULLY. POST INSPECTION AIRCRAFT WAS RUN UP AND NO CAUTION OR ADVISORY LIGHTS ILLUMINATING. ALL SYSTEMS PERFORMING NORMALLY. AIRCRAFT WAS PLACED ON MEL AND FLOWN UN-PRESSURIZED TO KRGK. AN INSPECTION OF DOOR SEAL AND DOOR SEAL AREA WAS PERFORMED WITH NO INDICATIONS OF TEARS OR HOLES IN DOOR SEAL. SUSPECTED WATER ENTRAPMENT IN CABIN DOOR SEAL. DOOR SEAL WAS BLOWN OUT AND WATER WAS REMOVED FROM THE INTERIOR OF THE SEAL. SUSPECT WATER FROZE INSIDE SEAL AND COULD NOT FORM TO CABIN DOOR FRAME FOR PROPER PRESSURIZATION.