N560TA

CESSNA 560 · 1997 · Valid Registration

Registered owner: CU III LLC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
PREMIER AIR, INC. (2RPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2024-03-24 Matched by certificate designator
ATA 5210

3/24/24 N560TA DEPARTED KFLL TO KHYA. CRUISING AT FL390 THE CREW HEARD A LOUD WHISTLE COMING FROM THE DOOR SEAL. THE CREW NOTICED THAT THE CABIN ALTITUDE WAS CLIMBING AND ASKED FOR A DESCENT. COMING TO FL240 THE CABIN PRESSURE WOULD NOT STABILIZE AND BEGAN TO CLIMB. THE CREW-INITIATED CABIN DECOMPRESSION CHECKLIST AND ASKED FOR ALT 10,000 FROM ATC WHILE DIVERTING TO KCHS. ONCE AT ALT 10,000 THE CABIN STABILIZED, AND THE CREW DOWNGRADED THE EMERGENCY AND LANDED IN KCHS WITH NO FURTHER ISSUES. MAINTENANCE REPLACED DOOR SEAL WITH NEW AND OPERATIONAL CHECK GOOD AT THIS TIME.

Source: SDR 2RPA2024032700005 · FAA SDRS
J · 2023-11-11 Matched by certificate designator
ATA 2210

APPROXIMATELY 1 HR INTO FLT AT FL410, AUTOPILOT DISCONNECTED WITHOUT ANY AURAL IND. ATTEMPTED TO RE-ENGAGE AUTOPILOT BUT DID NOT ENGAGE. NO ANNUNCIATED FD MODES & SEVERAL UNSUCCESSFUL ATTEMPTS WERE MADE TO SELECT ROLL & PITCH MODES WITH FD CONTROL PANEL. FD COMMAND BARS ON PILOT’S EADI REMAINED OUT OF VIEW. PILOT’S EHSI SHOWED A RED X ACROSS INSTRUMENT & APPEARED HEADING INFO NOT VALID. PILOT RESUMED MANUAL HAND-FLYING ACFT RELYING ON STDBY INST. CO-PILOT’S FD REMAINED IN VIEW BUT HAD NO WAY OF SETTING HEADING USING HEADING BUG, IT WAS NOT OPERABLE VIA REMOTE CONTROLLER. NO VISIBLE HEADING BUG ON PILOT’S PFD OR MFD. NO PRESELECT ALTITUDE VALUE VISIBLE ON PILOT’S PFD OR MFD, ONLY DASHES. PILOT ATTEMPTED TO REVERT TO CO-PILOT’S HEADING SYS, USING HEADING REVERSION BUTTON, NO SUCCESS. MFD DISPLAYED “MENU INOP. DECISION MADE TO DECLARE AN EMERGENCY & DIVERT TO KCLT WHERE VFR WX REPORTED & A VISUAL APPROACH CONDUCTED. A NORMAL LANDING MADE IN KCLT. MX FOUND EFIS CONTL 1 C/B TRIPPED. RESET BREAKER & OPS CHKD A/P & OTHER SYS & COULD NOT DUPLICATE FAILURE. WHEN DESCRIBING THE EVENTS TO MAINTENANCE, ONE OF THE ITEMS THE PILOT MENTIONED WAS AN ISSUE WITH THE PILOTS PUSH TO TALK SWITCH NOT WORKING. AT THE TIME IT WAS BELIEVED TO BE UNRELATED TO THE AVIONICS ISSUE BUT WE DID HAVE MAINTENANCE CHECK IT. THEY COULD NOT DUPLICATE ANY ISSUE WITH IT AND FOUND IT TO OPERATE NORMALLY. THE NEXT DAY WHEN THE CREW WAS PREPARING TO DEPART THEY REPORTED IT WASN’T WORKING AGAIN SO IT WAS DEFERRED PER THE MEL. IT WAS LATER DETERMINED THAT THE REASON THE SWITCH WAS INTERMITTENT WAS BECAUSE IT WAS GETTING PRESSED TOO DEEP INTO THE YOKE SWITCH BUSHING. IF THE SWITCH WAS PRESSED TOO HARD IT WOULD COME INTO CONTACT WITH THE AUTO-PILOT DISCONNECT SWITCH CONTACT IN THE YOKE AND TRIP THE CB.

Source: SDR 2RPA2023111100004 · FAA SDRS
N · 2022-11-24 Matched by certificate designator
ATA 3150

AT FL 410 "DOOR SEAL" ANNUNCIATOR ILLUMINATED. SHORTLY AFTER THAT CABIN ALTITUDE STARTED CLIMBING 5000-6000 FT PER MINUTE. PERFORMED EMERGENCY DECENT WITH OXYGEN ON. DECLARED EMERGENCY AND DESCENDED TO 9000 FT. UPON INSPECTION OF ALL ASSOCIATED COMPONENTS THAT MAKE UP THE DOOR SEAL SYSTEM, NO PHYSICAL DAMAGE TO ANY PARTS WERE NOTED. CONNECTED TO SERVICE AIR MAINTENANCE PORT AND PURGED WITH DRY NITROGEN. OBSERVED THE ACTUATION OF THE MAIN DOOR CABIN SEAL WITH NO DEFECTS NOTED. BOTH DOOR ANNUNCIATORS WERE CHECKED FOR PROPER RIGGING. SUSPECT MOISTURE IN THE SERVICE AIRLINE DUE TO MOISTURE THAT WAS INITIALLY FOUND AROUND THE DOOR HINGE UPON OPENING THE DOOR ON GROUND.

Source: SDR 2RPA2022120100001 · FAA SDRS