N563CS

CESSNA 560XL · 2005 · Valid Registration

Registered owner: TULSA XLS LLC, OK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-12-05 Matched by certificate designator
ATA 2910

THE FLIGHT CREW REPORTED A STABILIZER MISCOMPARE ANNUNCIATOR ILLUMINATED WHEN COMMANDING FLAPS 0 TO 15 FOLLOWED THE QRH WHICH LED THE CREW PULLING THE STAB CONTROL CIRCUIT BREAKER. HYDRAULIC PRESSURE ANNUNCIATOR WAS FLASHING DUE TO STAB NOT MOVING. THE LANDING WAS UNEVENTFUL. THE BASE MAINTENANCE TEAM DETERMINED THE AIRSPEED SWITCH WAS DEFECTIVE. THE SWITCH WAS REMOVED AND REPLACED WITH NEW UNIT. OPS AND LEAK CHECKS WERE SATISFACTORY.

Source: SDR 9JLA2022121632678 · FAA SDRS
N · 2022-10-25 Matched by certificate designator
ATA 2613

THE FLIGHT CREW REPORTED THAT THE APU SHUTS DOWN WHEN BLEED AIR LOAD WAS APPLIED. THE MAINTENANCE TEAM VERIFIED DISCREPANCY AND FOUND THE APU INLET TEMP SENSOR DEFECTIVE. THE SENSOR WAS REMOVED AND REPLACED WITH A NEW UNIT. OPS CHECKS WERE SATISFACTORY, AND THE AIRCRAFT WAS RETURNED TO SERVICE

Source: SDR 9JLA2022102832674 · FAA SDRS
N · 2022-10-12 Matched by certificate designator
ATA 3297

THE FLIGHT CREW REPORTED THAT THE POWER BRAKE CIRCUIT BREAKER WOULD TRIP INTERMITTENTLY. THE MAINTENANCE BASE DETERMINED THAT THE POWER BRAKE CIRCUIT BREAKER WAS DEFECTIVE. THE CIRCUIT BREAKER WAS REMOVED AND REPLACED WITH A NEW BREAKER. OPERATIONAL CHECKS WERE SATISFACTORY, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022101432669 · FAA SDRS
N · 2022-08-16 Matched by certificate designator
ATA 2612

THE MAINTENANCE TEAM DISCOVERED DURING POSTFLIGHT CHECKS THE APU FIRE ANNUNCIATOR WOULD NOT ILLUMINATE DURING TEST. THE APU SYSTEM WAS DISABLED AND THE MAINTENANCE WAS DEFERRED, OPERATIONS CONTINUED UNDER MEL 49-20-01. DURING THE MAINTENANCE CORRECTIVE ACTIONS, THE MAINTENANCE TEAM DETERMINED THE APU FIRE LOOP SENSOR WAS DEFECTIVE. THE UNIT WAS REMOVED AND REPLACED WITH A NEW SENSOR. OPS CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022082332666 · FAA SDRS
L · 2022-07-29 Matched by certificate designator
ATA 2697

THE MAINTENANCE TEAM DISCOVERED DURING PREFLIGHT CHECKS THAT THE APU FIRE LED LIGHT WAS INOP DURING APU FIRE TEST. THE SYSTEM FAULT WAS DEFERRED UNDER MEL 49-20-01 AND OPERATIONS WERE CONTINUED UNTIL MAINTENANCE COULD BE SCHEDULED. THE MAINTENANCE PROVIDER TROUBLESHOT THE FIRE CONTROL SYSTEM AND REPLACED THE APU MNTR PCB (NZ026) WITH A NEW CONDITION PCB. OPS CHECKS GOOD, APU FIRE DETECT TEST AND APU FIRE SWITCH LIGHT TEST GOOD. THE AIRCRAFT WAS RETURNED TO SERVICE

Source: SDR 9JLA2022081132664 · FAA SDRS
K · 2022-07-07 Matched by certificate designator
ATA 3240

DURING POST FLIGHT CHECKS THE MAINTENANCE TEAM DISCOVERED BRAKE FLUID LEAKING FROM THE BRAKE BOOST PUMP FILTER HOUSING. THE MAINTENANCE TEAM REMOVED AND REPLACED THE BRAKE BOOST PUMP FILTER HOUSING O-RING PER THE AMM. LEAK CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022071232657 · FAA SDRS
J · 2021-10-02 Matched by certificate designator
ATA 3010

THE FLIGHT CREW REPORTED THE RIGHT SIDE HORIZONTAL STABILIZER PNEUMATIC BOOT FAILS TO INFLATE AND HAS ASSOCIATED YELLOW MASTER CAUTION WHEN IN AUTO OR MANUAL MODES. CREW NOTED A BUBBLE AND AREA NOT INFLATING ON UPPER INBOARD AREA OF BOOT. THE MAINTENANCE TEAM CONFIRMED THE DISCREPANCY AND REPLACED THE RIGHT HORIZ STAB TAIL DEICE BOOT WITH NEW. OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021100717376 · FAA SDRS
J · 2021-09-06 Matched by certificate designator
ATA 7414

THE FLIGHT CREW REPORTED THE LEFT IGNITOR WOULD NOT TURN OFF INDICATING THAT THE CADENCE OF IGNITOR FIRING IS NOT NORMAL. THE MAINTENANCE VENDOR TROUBLESHOT AND REPLACED THE LEFT ENGINE IGNITION RELAYS KZ051, KZ053 AND KZ055. ENGINE GROUND RUNS WERE SATISFACTORY, NO OTHER DEFECTS NOTED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021090817375 · FAA SDRS
S · 2021-08-18 Matched by certificate designator
ATA 7400

THE FLIGHT CREW REPORTED THAT DURING STARTING OF THE LEFT ENGINE FOR FLIGHT THE IGNITORS WOULD NOT TURN OFF. THIS CAUSED THE CREW TO SHUT THE ENGINE DOWN AND CANCELLING THE FLIGHT. THE MAINTENANCE TEAM DETERMINED THE KZ051 (P/N M6106/19-012) WAS DEFECTIVE. A NEW RELAY WAS INSTALLED. OPS CHECKS OF THE LEFT ENGINE IGNITION WAS SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE

Source: SDR 9JLA2021090217373 · FAA SDRS
O · 2021-08-18 Matched by certificate designator
ATA 7497

THE FLIGHT CREW REPORTED THE LEFT ENGINE IGNITORS WOULD NOT TURN OFF. THE MAINTENANCE TEAM DETERMINED THAT THE KZ051 RELAY CONTROLLING THE SYSTEM WAS AT FAULT. THE RELAY WAS REPLACED WITH A NEW UNIT AND OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021082017373 · FAA SDRS
J · 2021-06-14 Matched by certificate designator
ATA 5210

THE FLIGHT CREW REPORTED THAT DURING CLOSING THE CABIN DOOR FOR FLIGHT THE CABIN DOOR ANNUNCIATOR REMAINED ILLUMINATED. THE SCHEDULED FLIGHT WAS CANCELLED. THE MAINTENANCE VENDOR REPLACED THE DEFECTIVE MAIN DOOR VENT SOLENOID WITH AN NEW SOLENOID RIGGED AND RETURNED TO SERVICE. UPON PREFLIGHT FOR RETURN TO SERVICE IT WAS FOUND THAT THE NEW VENT SOLENOID HAD FAILED AND REQUIRED TO BE REPLACED. A SECOND NEW DOOR VENT SOLENOID WAS INSTALLED AND RIGGED BY THE MAINTENANCE VENDOR. FUNCTIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE. THIS REPORT OF A FAILED DOOR VENT SOLENOID FOLLOWS MANY OTHER SDR REPORTING OF THIS COMPONENT.

Source: SDR 9JLA2021061817366 · FAA SDRS
L · 2021-02-01 Matched by certificate designator
ATA 3260

THE FLIGHT CREW REPORTED THAT THE LANDING GEAR WARNING HORN WOULD NOT TEST ON ROTARY CHECK. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THAT THE ROTARY TEST SWITCH WAS DEFECTIVE. THE SWITCH WAS REPLACED WITH A NEW UNIT. OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021020411098 · FAA SDRS
J · 2017-08-23 Matched by certificate designator
ATA 5210

THE FLIGHT CREW REPORTED THAT DURING THE MAIN CABIN DOOR CLOSURE FOR FLIGHT THEY RECEIVED AN WARNING ANNUNCIATOR THAT THE MAIN CABIN DOOR VENT DOOR WAS INOPERATIVE. THE CABIN DOOR VENT SOLENOID WAS FOUND TO BE DEFECTIVE AND WAS REPLACED WITH A NEW UNIT.

Source: SDR 9JLA2017083113068 · FAA SDRS