N568EA

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2008-12-29 Matched by certificate designator
ATA 3411

CREW REPORTED AIRSPEED MISCOMPARES, ALTITUDE MISCOMPARES, STICK PUSHER FALL CAS MESSAGES IN FLIGHT. AIRSPEED INDICATIONS VARIED ACROSS ADC 1,2, AND 3 BY 20-30 KNOTS. ALTITUDE VARIED BY 200-300 FT, AUTOPILOT SYSTEM BECAME INOPERATIVE AFTER CAS MESSAGES, ACFT DEPARTED, FLIGHT CONDITIONS WERE DAY VMC. (K)

Source: SDR L412009F00000 · FAA SDRS
O · 2008-09-11 Unresolved
ATA 5340

A POPPING NOISE COMING FROM THE VICINITY OF THE CO PILOTS WINDOW. SIDE WINDOW RETAINERS WERE REPLACED.

Source: SDR 2008FA0000759 · FAA SDRS
O · 2008-07-03 Matched by certificate designator
ATA 2140

PILOT REPORTED A BLEED AIR TEMP OVERHEAT CAS MESSAGE DURING NORMAL FLIGHT. DURING GROUND TESTING, FOUND THE VORE WOULD NOT ACTUATE. THE ACTUATOR APPEARED TO BE MISADJUSTED. A POSSIBLE CAUSE WAS A MISADJUSTED VORE DOOR ACTUATOR. VERIFYING PROPER CALIBRATION OF ACTUATOR COULD PROLONG LONGEVITY. THERE WAS ALSO MOISTURE COLLECTING IN FAIRING BELOW THE ACTUATOR MOTOR. THIS COULD CONTRIBUTE TO MOISTURE COLLECTING IN THE ACTURATOR. IT APPEARED THAT SOME MOISTURE HAD COLLECTED AROUND THE END SHAFT OF THE ACTUATOR AND THE LOWER MOTOR BODY SCREWS. RECOMMEND HAVING A METHOD OF DRAINING MOISTURE FRO COLLECTING IN FAIRING. (K)

Source: SDR L412008F00000 · FAA SDRS