N568PA

GATES LEARJET CORP. 35A · 1978 · Valid Registration

Registered owner: CFF AIR INC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
PHOENIX AIR GROUP INC (ESPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

X · 2023-07-17 Matched by certificate designator
ATA 7321

DURING CRUISE, RH ENGINE EXPERIENCED A FLAMEOUT. THE FLIGHT CREW SECURED THE MOTOR AND RETURNED TO BASE. MAINTENANCE PERSONNEL REMOVED AND REPLACED THE RH FUEL CONTROL AND FUEL FILTER, PERFORMED FUEL PUMP FUNCTIONAL TESTS, AND PERFORMED FIVE POINT RUNS WITH ACES SPECTRAL ANALYZER. AIRCRAFT WAS RETURNED TO SERVICE 7/20/2023.

Source: SDR ESPA2023072400308 · FAA SDRS
K J · 2013-01-15 Matched by certificate designator
ATA 2910

AFTER TAKEOFF PILOT REPORTED NO HYD PRESSURE. UPON LANDING SAFELY AND TROUBLESHOOTING THE ISSUE , FOUND THE MLG ACTUATOR RETRACT SWIVEL FITTING HAD FAILED. R & R THE SWIVEL FITTING WITH A NEW PART (PN 142870). PERFORMED ALL GEAR SWINGS AND ASSOCIATED HYD CHECKS IAW WITH THE MM.

Source: SDR 2013F00018 · FAA SDRS
B J · 2008-11-17 Matched by certificate designator
ATA 7597

ON LIFT OFF, CREW NOTED FUMES AND SMOKE IN ACFT, AND THE ACFT PRESSURIZATION SYS WAS IN EMERGENCY. POWER WAS REDUCED AND ENGINE BLEED AIR SWITCHES WERE CYCLED, BUT LT ENGINE REMAINED IN EMERGENCY. CAPTAIN DECLARED AN EMERGENCY TO GET PRIORITY LANDING AND RETURNED WITHOUT INCIDENT. A MECHANIC WAS DISPATCHED, AND TROUBLESHOOTING REVEALED A BROKEN WIRE ON THE LT ENGINE BLEED CONTROL SWITCH LOCATED ON THE CO-PILOT`S INSTRUMENT PANEL. WIRE WAS REPAIRED AND SYS TESTED NORMALLY ON THE GROUND AND SUBSEQUENT TEST FLIGHT.

Source: SDR ESPADJ2008-2 · FAA SDRS
O · 2008-07-05 Matched by certificate designator
ATA 2497

(30) MINUTES AFTER THE ACTIVATION OF WINDSHIELD HEAT, THE RT ESSENTIAL BUS CIRCUIT BREAKER POPPED. CREW COMPLETED EMERGENCY CHECKLIST FOR AN ELECTRICAL FAILURE. THE CIRCUIT BREAKER WOULD NOT RESET. ATC GAVE VECTORS AND DESCENT. CREW DID A VISUAL APPROACH. NO EMERGENCY WAS DECLARED BY THE FLIGHT CREW, AIRPLANE LANDED WITHOUT INCIDENT. (K)

Source: SDR ESP2008F00000 · FAA SDRS
B · 2004-02-25 Matched by certificate designator
ATA 2120

SMOKE WAS SUSPECTED IN CABIN. ENTIRE AREA IN SUSPECTED AREA WAS INSPECTED. NO DEFECTS WERE FOUND. PILOT REPORTED LEADING EDGE ANTI-ICE WAS INADVERTENTLY LEFT ON POSSIBLE CAUSING THE SMELL OF SMOKE. AIRCRAFT WAS RUN, SYSTEMS WERE OPERATIONALLY CHECKED AND FOUND TO BE GOOD.

Source: SDR ESPA · FAA SDRS