N575EW
Operators of this aircraft
Who operated this tail, and how firmly we know it.
No operator established for this aircraft.
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
IN THE PROCESS OF TROUBLESHOOTING A PITCH PUMPING PROBLEM, A REPLACEMENT PITCH SERVO WAS INSTALLED. AS SOON AS POWER WAS APPLIED TO AIRCRAFT, THE AUTOPILOT CIRCUIT BREAKER TRIPPED. THE SERVICEABLE SERVO WAS FOUND TO HAVE PIN A, THE +28 VOLT MOTOR INPUT FOR CCW ROTATION, WAS INTERNALLY SHORTED TO THE CASE OF THE SERVO. THIS SAME INCIDENT OCCURRED ON MARCH 3, 2010 WITH A REPLACEMENT SERVO FROM THE SAME REPAIR STATION. THE FIRST INCIDENT DAMAGED THE AUTO PILOT COMPUTER BEFORE THE CIRCUIT BREAKER TRIPPED. RECORD CHECKS REVEALED THIS SERVO TO BE THE SAME ONE FROM THE PREVIOUS INCIDENT. FOLLOWING THE FIRST INCIDENT THE REPAIR STATION WAS CONTACTED AND GIVEN A DETAILED DESCRIPTION OF THE FAILURE, TO INCLUDE THE SHORT BETWEEN PIN A AND THE CASE. THE REPAIR REPORT THAT ACCOMPANIED THE SERVO WAS DATED MARCH 7, 2010 STATES DEAD SHORT, FAILED ON INSTALL, BURNED AP COMPUTER. THE DISPOSITION STATES FINAL TESTED OK, RECERTIFY UNIT AND RETURN TO SERVICEâ AND IS DATED MARCH 15, 2010. THIS SUBMITTER BELIEVES THAT THE SERVO TEST FIXTURES AND CONNECTOR BACKSHELLS NEED TO BE GROUNDED IN ORDER TO ENSURE THAT THIS TYPE OF FAULT IS DISCOVERED PRIOR TO RETURNING A PART TO SERVICE.