N586ND

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
University of North DakotaOperatoron 2012-08-01Operator named in NTSB report

Accident & incident history

Acc · 2012-08-01 Operator named in NTSB report
PIPER PA-44-180 None injury Part 91University of North Dakota
Source: NTSB case CEN12LA516

Maintenance disclosures

Service Difficulty Reports filed with the FAA for this airframe. Filing is largely voluntary — the number of reports is not a measure of reliability. To verify a report, search its control number at the FAA SDRS site.

4 reports on file, 2012-05-07 – 2015-02-13.

FLUID LOSS · 2015-02-13 Unresolved
ATA 3213

Part: STRUT — LEAKING (MLG) · airframe 2,066 hrs

DURING PHASE INSPECTION MECHANIC NOTED BOTH MLG STRUTS LEAKING FLUID. UPON DISASSEMBLY TO REPACK STRUTS MECHANIC FOUND APPROXIMATELY .5 CUP OF ALUMINUM SHAVINGS IN INNER STRUT. FURTHER INSPECTION FOUND OUTER STRUT INNER BORE GROOVED AND GOUGED IN THE AREA OF UPPER BEARING TRAVEL. UPPER BEARING ON BOTH STRUTS SHOWED ROUGH, SHARP EDGES WHERE IT CONTACTS OUTER STRUT. OUTER STRUT AND UPPER BEARING REPLACED WITH NEW PARTS. MFG CONTACTED.

Source: SDR 2015FA0000061
PARTIAL RPM/PWR LOSS · 2015-01-26 Unresolved
ATA 7414

Part: DISTRIBUTOR GEAR — DETACHED (RT MAGNETO) · airframe 2,045 hrs

AT RUN-UP, FOUND EXCESSIVE MAGNETO DROP ON LT ENGINE, RT MAGNETO. REMOVED MAGNETO AND FOUND DISTRIBUTOR FINGER LOOSE ON DISTRIBUTOR GEAR. THIS IS A COMMON FAILURE. REPLACED MAGNETO WITH SERVICEABLE MAGNETO.

Source: SDR OG5S2015FA0000041
PARTIAL RPM/PWR LOSS · 2014-12-01 Unresolved
ATA 7414

Part: DISTRIBUTOR GEAR — DETACHED (RT MAGNETO) · airframe 1,969 hrs

RIGHT MAGNETO, RT ENGINE OPERATED INTERMITTENTLY. REMOVED AND DISASSEMBLED. FOUND DISTRIBUTOR FINGER LOOSE ON DISTRIBUTOR GEAR. THIS IS A COMMON PROBLEM. INSTALLED SERVICEABLE MAGNETO.

Source: SDR OG5S2015FA0000042
PARTIAL RPM/PWR LOSS · 2012-05-07 Unresolved
ATA 6120

Part: OIL CAP — LOOSE (GOVERNOR) · airframe 926 hrs

AFTER LEVELING OFF AT 5,500 MSL THE CREW BEGAN LEANING MIXTURES AND THE RT ENGINE RPM BEGAN TO DROP AT A STEADY RATE. NO ENGINE ANNUNCIATORS APPEARED AND ALL ENGINE INSTRUMENTS READ NORMAL AFTER 15 SECONDS THE RT PROP WENT FULL FEATHER AND THE ENGINE WAS SHUTDOWN BY THE CREW. THEY RETURNED TO THE AIRPORT AND LANDED WITHOUT INCIDENT, ON ONE ENGINE. MX INSPECTED ACFT AND FOUND THE RT GOVERNOR WAS LEAKING AT THE TOP OF THE GOVERNOR BODY. GOVERNOR WAS REPLACED AND ALL SYS CHECKED GOOD. GOVERNOR WAS SENT TO OVERHAUL FACILITY FOR TEAR DOWN AND REPORT OF INTERNAL CONDITION. UPON TEARDOWN A ROTATION OIL PLUG IN THE BODY HAD CAME LOOSE AND OUT OF BODY CAUSING GOVERNOR TO LOOSE OIL PRESSURE. DURING DISCUSSION WITH OVERHAULER HE STATED THAT HE HAD NEVER SEEN THIS HAPPEN BEFORE.

Source: SDR 2012FA0000282