N5891V

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2015-08-03 Matched by certificate designator
ATA 8011

BENDIX ON STARTER OF RT ENGINE FAILED TO DISENGAGE AFTER STARTUP. R & R STARTER WITH NEW. NO FURTHER DISCREPANCIES NOTED.

Source: SDR RI9A20150809001 · FAA SDRS
O · 2014-12-22 Unresolved
ATA 8520

ENGINE RECEIVED FOR O/H DUE TO HIGH METAL. DURING DISASSEMBLY, IT WAS DISCOVERED THAT A PIECE OF THE CHEEK ON THE CRANKSHAFT HAD BROKEN OFF ALLOWING THE COUNTERWEIGHT TO IMPACT CONNECTING RODS AND THE CRANKSHAFT. THE COUNTERWEIGHT PINS WERE UNDAMAGED. THE CRANKSHAFT COUNTERWEIGHT BUSHING WAS BROKEN.

Source: SDR WS9R2015FA0000008 · FAA SDRS
K E · 2012-08-05 Unresolved
ATA 8520

PILOT HEARD RIGHT ENGINE RUNNING ROUGH AND SAW THE OIL PRESSURE DROP. SHUT THE ENGINE DOWN AND MADE A SAFE LANDING AT OUZINKIE AIR STRIP. UPON INSPECTION FOUND A CRACK IN THE CRANKCASE BETWEEN THE NR 3 AND NR 5 CYLINDERS. A NEW ENGINE WAS INSTALLED. AFTER REPAIRS THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR RI9A20120807557 · FAA SDRS
B · 2012-06-06 Matched by certificate designator
ATA 2436

PILOT SMELLED ODOR AND SAW SMOKE FROM INSTRUMENT PANEL. PILOT RETURNED TO KODIAK AIRPORT WITHOUT INCIDENT AND MADE A NORMAL LANDING. ON INVESTIGATION, IT WAS FOUND THE RIGHT ENGINE ALTERNATOR VOLTAGE REGULATOR HAD CAUSED AN OVERVOLTAGE SITUATION AND THE SMOKE WAS CAUSED BY THE BATTERY BEING OVERCHARGED. A NEW REGULATOR WAS INSTALLED. THE OVERVOLTAGE ALSO CAUSED SEVERAL ENGINE INDICATING INSTRUMENTS TO BE REPLACED. AFTER REPAIRS, THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR RI9A20120617001 · FAA SDRS