N58HJ

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Eagle Helicopters, Inc. (HEAA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 1998-05-03 Matched by certificate designator
ATA 7250

IT WAS NOTED DURING OPERATION, ENGINE EGT WAS OBSERVED TO BE ABOVE NORMAL. UPON TEARDOWN OF HOT SECTION, THE FIRST STAGE TURBINE NOZZLE OUTER SHROUD WAS FOUND SEVERELY CRACKED. (X)

Source: SDR 98ZZZX2880 · FAA SDRS
O · 1997-11-13 Matched by certificate designator
ATA 7210

FOLLOWING DISASSEMBLY OF ENGINE FOR METAL CONTAMINATION, DISCOVERED 2 EACH OF THE LOCKCUPS HAD FAILED. CUPS CRACKED AND SPLIT AT THE LOCKING TANGS WHICH ENGAGE THE PLANETARY GEARSHAFTS. THE RETAINING NUTS WHICH THE LOCKCUPS RETAIN, REMAINED IN PLACE AND THE PIECES OF THE LOCKCUPS WERE FOUND IN THE SCAVENGE SCREEN OF THE ACCESSORY DRIVE GEARBOX AND LAYING IN THE OUTPUT REDUCTION GEARBOX.

Source: SDR 97ZZZX4895 · FAA SDRS
E · 1997-10-23 Matched by certificate designator
ATA 6410

WHILE CARRYING OUT OPERATIONS ON THE AFTERNOON OF 10-23-97, PILOT REPORTED INCREASE OF VIBRATION WHILE IN-FLIGHT RETURNING TO LANDING SITE. AIRCRAFT WAS SHUT DOWN. ON EXAMINATION OF TAIL ROTOR, INSIDE PART OF TIP WAS FOUND MISSING. NO OTHER DAMAGE WAS APPARENT AND SUBSEQUENT TAIL ROTOR REPLACMENT AND BALANCING CURED PROBLEM. (X)

Source: SDR 97ZZZX4824 · FAA SDRS
J · 1997-10-18 Matched by certificate designator
ATA 7261

PILOT REPORTED LOSS OF OIL PRESSURE IN-FLIGHT. THE FLIGHT WAS TERMINATED IMMEDIATELY AND THE ENGINE WAS SHUT DOWN. UPON INVESTIGATION, THE ENGINE OIL PUMP DRIVESHAFT WAS FOUND BROKEN. WHEN PUMP WAS REMOVED, A PIECE OF GEAR TOOTH FELL FROM PUMP OIL PASSAGE. GEAR PIECE IS FOREIGN TO THE OIL PUMP. AT THIS TIME, IT IS NOT KNOWN WHERE THE GEAR TOOTH CAME FROM.

Source: SDR 97ZZZX4823 · FAA SDRS