N597P

RAYTHEON AIRCRAFT COMPANY C90A · 2000 · Valid Registration

Registered owner: GUARDIAN FLIGHT LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
GUARDIAN FLIGHT, LLC. (G1IA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

M B · 2024-11-16 Matched by certificate designator
ATA 2140

WE HAD JUST LEVELED OFF AT 14,000' FOR CRUISE WHEN THE MED CREW REPORTED SMOKE AND THE SMELL OF SOMETHING BURNING IN THE CABIN. I LOOKED AND THERE WASN'T MUCH SMOKE, BUT IT WAS THERE. I COULD BARELY SMELL IT IN THE COCKPIT BUT IT APPEARED TO BE THICKER IN THE CABIN. THEY SAID IT KIND OF SMELLED LIKE A CROSS BETWEEN ELECTRICAL AND OVERHEATING HEATER. THEY WERE UNABLE TO LOCATE WHERE IT WAS COMING FROM. I TURNED THE HEAT ALL THE WAY DOWN AND THE SMOKE SEEMED TO DISSIPATE AFTER A FEW MINUTES. WE WERE OVER HALFWAY AT THAT POINT SO WE ELECTED TO CONTINUE ON TO KWRL. CORRECTIVE ACTION: WITH THE CABIN TEMP MODE AND VENT BLOWER IN “AUTO”, ELECTRIC GROUND HEAT IN “NORMAL”, AND THE CABIN TEMP SET TO “HIGH”, AND THE COCKPIT VENTS CLOSED AND CABIN AIR SET TO FULL DECREASE, EXCESSIVE HEAT AND MINIMAL AIR FLOW WAS FOUND AT THE REGISTERS. THIS CONFIGURATION MATCHED THE CONFIGURATION OF THE FLIGHT THAT PRODUCED A BURNING SMELL AND SMOKE. IN THIS CONFIGURATION ON THE GROUND, THE SMELL OF HOT PLASTIC WAS APPARENT, BUT THE CONFIGURATION WAS CHANGED BEFORE ANY SMOKE WAS PRODUCED. THE LIGHT SMOKE PRODUCED DURING FLIGHT WAS LIKELY THE RESULT OF FUZZ, LINT, AND OR DUST BUILT UP IN THE DUCTS, VALVES, AND PLENUM BEING EXPOSED TO THE HIGH HEAT OF THE ENVIRONMENTAL PLUMBING. INCREASING CABIN AIR AND OPENING COCKPIT VENTS IMMEDIATELY CAUSED THE TEMPERATURES AT THE REGISTERS TO DECREASE AND DISSIPATED THE HOT PLASTIC SMELL. THE CAUSE OF THE DISCREPANCY WAS FOUND TO BE CALLING FOR HIGH HEAT WITH ALL COCKPIT VENTS CLOSED AND CABIN AIR SET TO FULL DECREASE. NO DEFECTS FOUND AT THIS TIME.

Source: SDR G1IA20241116075 · FAA SDRS
J · 2024-10-15 Matched by certificate designator
ATA 3460

DISCREPANCY: SHORTLY AFTER TAKE OFF DPU FAIL INDICATION DISPLAYED ON BOTH EFIS SCREENS, THEN A FEW SECONDS LATER BOTH SCREENS WENT COMPLETELY BLANK EXCEPT FOR DPU FAIL MESSAGE. ABOUT TEN SECONDS LATER THE FAILURE INDICATIONS RESOLVED. CORRECTIVE ACTION: REMOVED DPU AND CLEANED CONNECTORS, OPS CHECK SATISFACTORY.

Source: SDR G1IA20241015072 · FAA SDRS
B · 2024-07-25 Matched by certificate designator
ATA 2100

NOTICED SPARKS MOVING BY LEFT SIDE WINDOW AFTER TAKEOFF. LEFT THE LANDING GEAR EXTENDED. MADE AN IMMEDIATE RTB TO RNW 29 AND LANDED SAFELY. PARKED AIRCRAFT ON RAMP, EVACUATED ALL PERSONNEL, MOVED AWAY FROM THE AIRCRAFT. SAW SMOKE AND FELT HEAT COMING FROM LEFT SIDE AIR CONDITIONER EXHAUST VENT.

Source: SDR G1IA20240725064 · FAA SDRS