N598JL

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2021-08-12 Matched by certificate designator
ATA 7830

THE FLIGHT CREW REPORTED THAT THE LEFT THRUST REVERSER LOCKED OUT OF REVERSING. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THE T/R LOCKOUT SOLENOID WAS FAULTY. THE DEFECTIVE SOLENOID WAS REMOVED AND A NEW UNIT WAS INSTALLED. OPERATIONAL CHECKS SATISFACTORY. AIRCRAFT WAS RETURN TO SERVICE.

Source: SDR 9JLA2021081633281 · FAA SDRS
B J · 2021-07-08 Matched by certificate designator
ATA 3140

THE FLIGHT CREW REPORTED THAT DURING PREFLIGHT CHECKS THE NO1 PRIMARY FLIGHT DISPLAY (PDF) CIRCUIT BREAKER TRIPPED. THE FDR FAIL ANNUNCIATOR ILLUMINATED, ELECTRICAL SMOKE AND SMELL IN THE DEVELOPED IN THE COCKPIT. THIS CAUSED THE SCHEDULED FLIGHT TO BE CANCELLED. THE MAINTENANCE TEAM DETERMINED THE NO1 PDF WAS DEFECTIVE AND WAS REMOVED. A TESTED/INSPECTED PDF WAS INSTALLED. OPS CHECKS WERE GOOD AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021072833274 · FAA SDRS
O · 2004-09-10 Unresolved
ATA 1430

RT MAIN TIRE SIDEWALL AND TREAD DEPARTED AIRCRAFT ON LANDING ROLLOUT. DETERMINED BROKEN WHEEL THROUGH BOLT DISLODGED INSIDE WHEEL HALF CAUSED BREAKAGE OF FUSIBLE PLUG AND EVENTUAL DEFLATION OF TIRE DURING FLIGHT. AIRCRAFT LANDED ON DEFLATED TIRE. (CE09200404725)

Source: SDR 2004FA0000740 · FAA SDRS
F · 2004-08-03 Unresolved
ATA 2210

(LG NR 000173) AIRCRAFT DEPARTED, CLIMBING THROUGH FL370 AT M.58, THE YAW DAMPER BEGAN A SERIES OF LT TO RT INPUTS INCREASING TO FULL SCALE DEFLECTION AT A RATE OF APPROXIMATELY ONE PER SECOND. THE AUTOPILOT WAS TURNED OFF, AND THE MALFUNCTION CONTINUED. TURNED YAW DAMP OFF, AND THE MALFUNCTION CEASED. CREW NOTIFIED ATC AND RETURNED TO AIRPORT. PHYSICAL LOCATION OF FAILED PART IS IN THE AFT TAIL CONE COMPARTMENT. (CE09200404353)

Source: SDR JX62004F00000 · FAA SDRS
J · 2004-01-22 Unresolved
ATA 3230

NOSE GEAR EXTENDED DURING DESCENT ON ITS OWN. EXTENDED GEAR, VERIFIED GEAR DOWN AND LOCKED, CONTINUED DESCENT TO ORIGINAL DESTINATION, LANDED WITHOUT EVENT. FOUND NLG UPLOCK MECHANISM OUT OF RIG. RE-RIG, LUBRICATE AND OP TEST SATISFACTORY.

Source: SDR RJ19002 · FAA SDRS
C · 2002-10-18 Unresolved
ATA 7200

DURING THE T/O ROLL AT APPROXIMATELY 30 KTS, A FUELING PAD (PAD USED BY THE FUELER TO PROTECT THE PAINT DURING FUELING) WAS INGESTED INTO THE NR 2 ENGINE. THE T/O WAS ABORTED AND ENGINE SHUT DOWN AFTER RETURNING TO FBO.LA - TEST

Source: SDR RJ19 · FAA SDRS