N60ES

CESSNA 750 · 1998 · Valid Registration

Registered owner: ESMARK AVIATION LLC, PA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CORPORATE AIR LLC (XCGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2014-03-18 Matched by certificate designator
ATA 5300

PILOT REPORTED COMM RADIOS UNUSABLE BELOW 130.000 MHZ WHILE IN FLIGHT. HIGH PITCHED SQUEAL INTERFERENCE HEARD. BACKUP HANDHELD TRANSCEIVER WAS ALSO AFFECTED IN THE SAME FREQUENCY RANGE. PILOTS SQUAWKED 7600 & PROCEEDED VFR IAW 14 CFR 91.185. PILOTS USED SAT PHONE TO CONTACT KMDW TOWER FOR FREQUENCY ABOVE 130.000 MHZ. RADIO COMM WERE RE-ESTABLISHED 10 MINUTES AFTER FAILURE & A NORMAL LANDING WAS MADE. UNABLE TO DUPLICATE PROBLEM, ALL RADIOS OPERATED NORMALLY. FOUND THE RADOME, THE NOSE GEAR & THE NOSE GEAR DOORS BONDING TO THE FUSELAGE TO BE UNSERVICEABLE. AFTER CLEANING THE BONDING SURFACES & REATTACHING THE BONDING HARDWARE THE AIRPLANE PASSED THE PRECIPITATION STATIC TEST.

Source: SDR XCGA20140322001 · FAA SDRS
Y J · 2013-09-20 Matched by certificate designator
ATA 7220

ON DESCENT, THE RIGHT ENGINE SHUTDOWN AND THE FADEC FAIL RT CAS MESSAGE ILLUMINATED. PILOTS ATTEMPTED TO RESET THE FADEC WITHOUT SUCCESS AND THEN COMPLIED WITH THE EMERGENCY CHECKLIST. THE AIRPLANE LANDED WITHOUT INCIDENT AND WAS TURNED OVER TO MX AT THE SERVICE CENTER. MFG`S DETERMINED AFTER TROUBLESHOOTING, THE INLET GUIDE VANE ACTUATOR HAD FAILED. THEY REPLACED THE ACTUATOR AND PERFORMED ALL REQUIRED OPS TESTS WITHOUT DISCREPANCY.

Source: SDR XCGA60ES92013 · FAA SDRS
B · 2013-07-08 Matched by certificate designator
ATA 2150

SEVERAL MINUTES AFTER LANDING, THE CREW WAS CLEANING THE AIRPLANE INTERIOR WHEN THEY NOTICED HOT AIR AND A BURNING SMELL COMING FROM THE CABIN VENTILATION SYS. SHORTLY THEREAFTER, SMOKE WAS OBSERVED AS A LIGHT HAZE IN THE CABIN. DESPITE BEING SELECTED TO A COOL SETTING, THE SUPPLY TEMPERATURE OF THE CABIN PACK IN THE COCKPIT INDICATED A TEMPERATURE OF OVER 210 DEGREES F WHICH WAS STEADILY CLIMBING UNTIL THE PAC WAS SELECTED OFF. AFTER SELECTING THE PAC OFF, THE SUPPLY TEMPERATURE STEADILY LOWERED AND THE SMOKE SUBSIDED. THE CABIN ACM PAC WAS DEFERRED IAW THE MEL AND THE AIRPLANE WAS FLOWN TO THE SERVICE CENTER. MX DISCOVERED THE CABIN ACM TO BE FROZEN. THE CABIN ACM WAS REPLACED DUE TO THE FAILURE, WE ALSO HAD THE COCKPIT ACM REPLACED AS A PREVENTIVE MEASURE.

Source: SDR XCGAN60ES07102013 · FAA SDRS