N60VP

RAYTHEON AIRCRAFT COMPANY C90A · 1998 · Valid Registration

Registered owner: GUARDIAN FLIGHT LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
GUARDIAN FLIGHT, LLC. (G1IA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-02-17 Matched by certificate designator
ATA 3260

ON APPROACH THE RH MLG DID NOT LOCK DOWN AND SHOW A GREEN LIGHT WHEN EXTENDED. THE GEAR WAS CYCLED BUT THERE WAS NO CHANGE IN INDICATIONS. MANUAL GEAR EXTENSION PROCEDURES WERE USED AND THREE GREEN LIGHTS WAS ACHIEVED BEFORE LANDING. R&R AND ADJUSTED RH DOWNLOCK SWITCH OPS CHECK GOOD, OCF SATISFACTORY

Source: SDR G1IA02172025085 · FAA SDRS
P S · 2025-01-31 Matched by certificate designator
ATA 3297

LANDING GEAR WOULD NOT EXTEND, LANDING GEAR C/B TRIPPED PUMPED GEAR DOWN AND RETURNED TO HNL, ( ACTION TAKEN ) PUMPED HANDLE BEFORE LANDING TO INSURE GEAR WAS DOWN

Source: SDR G1IA202501310083 · FAA SDRS
O · 2024-10-21 Matched by certificate designator
ATA 2121

AIR CONDITIONING NOT BLOWING COLD AIR IN AUTO OR MANUAL MODE. CORRECTIVE ACTIONS: REPLACED MOTOR WITH OVERHAULED. NOTE: AMT STATED THERE WAS A HOLE IN THE REMOVED MOTOR.

Source: SDR G1IA20241021073 · FAA SDRS
B · 2024-09-05 Matched by certificate designator
ATA 2150

AIR CONDITIONER DRIVE MOTOR PUTTING OFF SMOKE AFTER LANDING AND FOUND TO BE UNSERVICEABLE.

Source: SDR G1IA2024091005068 · FAA SDRS
K · 2021-01-08 Matched by certificate designator
ATA 2810

CREW NOTICED FUEL LEAKING FROM RIGHT HAND OUTBOARD WING FUEL CAP. AIRCRAFT RETURNED FROM DEPARTING AIRPORT (PHNL) AND THE FUEL CAP WAS REPLACED WITH A NEW CAP. THE AIRCRAFT HAS SINCE FLOWN 6 MORE LEGS (4.9 HOURS) WITH NO DEFECTS NOTED.

Source: SDR G1IA01112021 · FAA SDRS
B · 2018-10-02 Matched by certificate designator
ATA 2120

DURING CRUISE AT FL120 FROM KE91 TO KFLG PILOT AND CREW NOTED AN UNUSUAL SMELL, REPORTED AS A "HOT GLUE GUN SMELL". PILOT MADE A PRECAUTIONARY LANDING AT KINW WITHOUT INCIDENT. AIRCRAFT WAS INSPECTED AND EXTENSIVE GROUND RUNS WERE PERFORMED WITH NO DISCREPANCY OBSERVED. ALL SYSTEMS OPERATING AS EXPECTED AND NO UNUSUAL SMELLS PRESENT. AIRCRAFT WAS RELEASED FOR A CHECK FLIGHT WHICH WAS COMPLETED WITHOUT INCIDENT. AIRCRAFT WAS RETURNED TO SERVICE AND HAS HAD NO FURTHER REPORTS OF ANY UNUSUAL SMELLS.

Source: SDR G1IA2018100900001 · FAA SDRS
B · 2011-02-09 Matched by certificate designator
ATA 2121

ENVIROMENTAL BLOWER FAILED, SMOKE IN CABIN.

Source: SDR 9CC2011F00000 · FAA SDRS