N635QX

EMBRAER S A ERJ 170-200 LR · 2018 · Valid Registration

Registered owner: HORIZON AIR INDUSTRIES INC, WA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2026-05-03 Matched by certificate designator
ATA 5410

LEFT LEADING EDGE OVER PYLON IS CHAFED. REPAIRED IAW SRM 57-49-01 REPAIR 7. MATERIAL USED T024T3 .063"

Source: SDR QXEA2026051100104 · FAA SDRS
O · 2026-05-03 Matched by certificate designator
ATA 5410

RIGHT HAND LEADING EDGE AT PYLON IS CHAFED. REPAIRED IAW SRM 57-49-01 REPAIR 7. MATERIAL USED T024T3.

Source: SDR QXEA2026051100105 · FAA SDRS
O · 2026-04-30 Matched by certificate designator
ATA 5347

RIGHT HAND LATERAL SEAT TRACK AT FRAME 34-60 HAS GOUGES AND MISSING PAINT. BLENDED AND FOUND TO BE OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08, RESTORED FINISH.

Source: SDR QXEA2026051100107 · FAA SDRS
O · 2026-04-29 Matched by certificate designator
ATA 5347

LEFT HAND SEAT TRACK AT STATION 73-84 GOUGED AND MISSING PAINT. REWORKED AND FOUND TO BE OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08. RESTORED FINISH.

Source: SDR QXEA2026051100111 · FAA SDRS
O · 2026-04-29 Matched by certificate designator
ATA 5347

RIGHT HAND SEAT TRACK AT FRAME 44-84 HAS GOUGES AND MARKS AND MISSING PAINT. REWORKED AREA AND FOUND TO BE OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08. RESTORED FINISH.

Source: SDR QXEA2026051100110 · FAA SDRS
O · 2026-04-27 Matched by certificate designator
ATA 5347

RIGHT HAND SEAT TRACK AT STATION 60-74 HAS AREAS OF GOUGES AND MISSING PAINT. REWORKED AND FOUND TO BE OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08 RESTORED FINISH.

Source: SDR QXEA2026051100109 · FAA SDRS
O · 2026-04-27 Matched by certificate designator
ATA 5300

RIGHT HAND SEAT TRACK AT STATION 17-23 HAS CORROSION IN MULTIPLE SPOTS. REMOVED DAMAGED AREAS AND FOUND TO BE OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08 AND RESTORED FINISH.

Source: SDR QXEA2026051100108 · FAA SDRS
O · 2026-04-20 Matched by certificate designator
ATA 5300

FRAME 19 LBL 11 CORROSION AT SCRFW HOLE ON BEAM. AFTER REWORK FOUND TO BE OUT OF LIMITS. REPAIRED AREA IAW ARM 53-10-10-02-01. RESTORED FINISH.

Source: SDR QXEA2026051100113 · FAA SDRS
O · 2026-04-20 Matched by certificate designator
ATA 5330

DOUBLER AT FRAME 16 LBL 11 IS CORRODED. REMOVED DAMAGED AREAS AND FOUND TO BE OUT OF LIMITS. REPAIRED PER ETD 2026-170-006563.

Source: SDR QXEA2026051100112 · FAA SDRS
O · 2026-04-18 Matched by certificate designator
ATA 5347

RIGHT HAND LATERAL SEAT TRACK AT FRAME 73-75 HAS TOOLING MARKS DAMAGE FROM PREVIOUS WORK PERFORMED. BLENDED AREA BUT OUT OF LIMITS. REPLACED SEAT TRACK IAW SRM 51-40-08.

Source: SDR QXEA2026051100106 · FAA SDRS
J · 2025-11-17 Matched by certificate designator
ATA 2210

AUTOPILOT FAILED ON SHORT FINAL WITH AUTOLAND SETUP ON APPROACH. RESULTING IN MISSED APPROACH. LANDING UNEVENTFUL. REMOVED FROM SERVICE. NO FAULTS ON EICAS. INTEROGATED CMC FOUND FAULT CODE 27030348FCS IN HISTORY VIEW. PERFORMED FIM MCN E270027 COMPLETED THROUGH SUB TASK 27-03-00-813-466-A(QX) NO FAULTS TRANSITORY CONDITION OF FLIGHT CTRL SYS. NO FURTHER MAINT ACTION REQUIRED. ALL OPS CHECKS PER FIM CHECKED OKAY. PERFORMED AUTOPILOT OPS TEST PER AMM 22-11-001-710-802-A. OPS TEST GOOD NO DEFECTS NOTED. AIRCRAFT REMAINS CAT III. FLIGHT DECK PLACARD READS CAT III, RETURNED TO SERVICE. NO PARTS REPLACED.

Source: SDR QXEA2025111799344 · FAA SDRS
O · 2025-07-13 Matched by certificate designator
ATA 7320

PER ECMP REQUEST REPLACE THE #1 FADEC WITH POBIT. FADEC REPLACED.

Source: SDR QXEA2025071400275 · FAA SDRS
O · 2025-06-22 Matched by certificate designator
ATA 3830

FLIGHT 2117. BOTH LAVS WOULD NOT FLUSH DURING FLIGHT. LAV TANK LIGHT INDICATES FULL. DIVERTED AND MADE A UNEVENTFUL LANDING. REMOVED WASTE TANK FULL-LEVEL SENSOR. INSPECTED AND FOUND WASTE-TANK "FULL" LEVEL SENSOR TO BE DIRTY. CLEANED AND REINSTALLED SENSOR IAW E175 AMM 38-32-20-000/400-801-A. INSTALLED NEW O-RING REF MCN E380003-001 ISSUE 1. OPS TEST: GOOD. NO FURTHER DEFECTS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2025062300265 · FAA SDRS
J · 2025-05-06 Matched by certificate designator
ATA 7321

ENG 2 SHORT DISPATCH ADVISORY ON EICAS. REMOVED FROM SERVICE. INTERROGATED CMC FOUND RELATED SHORT DISPATCH F/C:73217422G2A PER GE LMM FAULT ISOLATION TASK 72-00-00-810-808 SUBTASK 72-00-00-810-133 REMOVED AND REPLACED ENGINE 2 FADEC IAW AMM 73-21-01-000/400-801-A OPS CHECKS NORMAL. SHORT DISPATCH CLEARED, NO FURTHER DEFECTS NOTED. A/C OK FOR CONTINUED SERVICE.

Source: SDR QXEA2025050900174 · FAA SDRS
K · 2025-03-13 Matched by certificate designator
ATA 2810

FLIGHT 2069. NOTED POSSIBLE FUEL LEAK IN WING TO FUSELAGE FIARING AREA ABOUT 6" FROM L/H WHEEL WELL FORWARD BULKHEAD. PLACED ON DMI 1087563 TO BE COMPLETED WITHIN 600 HOURS.

Source: SDR QXEA2025031700062 · FAA SDRS
L · 2024-12-25 Matched by certificate designator
ATA 3350

PILOT REPORTED PHOTOLUMINESCENT INDICATOR STRIP LIGHT AT 1B/2B VARIOUS INOP SPOTS. REMOVED FROM SERVICE. REPLACED LIGHT STRIP. OPERATIONAL CHECKS GOOD RETURNED TO SERVICE.

Source: SDR QXEA2024122700324 · FAA SDRS
W · 2024-11-22 Matched by certificate designator
ATA 2565

FLIGHT 2250. WHEN RAMPERS OPENED L1 DOOR FROM OUTSIDE, GIRT BAR REMAINED ATTACHED AND SLIDE CAME PART WAY OUT OF BUSTLE REMOVED FROM SERVICE. FERRIED FOR REPAIRS. C/W LIVE DOOR GUIDANCE MCN E250094-0. REMOVED DOOR BUSTLE, GIRT BAR AND SLIDE ASSY IAW AMM 25-65-01-000-801-A. VERIFY DOOR IS CLOSED AND LOCKED AND INDICATES AS SUCH. DOOR LABLED”INOPERATIVE DO NOT USE FOR EGRESS”. I HAVE PERFORMED ALL INSPECTIONS AND/OR TESTS AS DETAILED IN PARAGRAPH C OF THIS FERRY PERMIT AND HAVE DETERMINED THAT THE AIRCRAFT IS SAFE FOR FERRY FLIGHT. AIRCRAFT REMAINS OUT OF SERVICE.

Source: SDR QXEA2024112200279 · FAA SDRS
O · 2024-11-17 Matched by certificate designator
ATA 3241

AUTOBRAKE KNOB WON'T STAY IN RTO POSITION (AUTOBRAKE SYSTEM - DEACTIVATED). REMOVED FROM SERVICE. C/W E175 FIM TASK 32-41-00-810-810-A STEP 7. L. (2). REMOVED AND REPLACED THRUST CONTROL QUADRANT ASSY REF E175 AMM TASK 76-11-01-000-801-A AND 76-11-01-400-801-A. OPS CHECK GOOD. PERFORMED MAIN BRAKE AUTO-BRAKE SYSTEM FUNCTIONAL TEST REF E175 AMM TASK 32-41-02-720-801-A. OPS CHECK GOOD. RETURNED TO SERVICE.

Source: SDR QXEA2024111800277 · FAA SDRS
O · 2024-10-19 Matched by certificate designator
ATA 3350

TRIM PIECE BROKE OFF EXIT SIGN AT L1 DOOR. REMOVED FROM SERVICE. REMOVED AND REPLACED FWD EXIT IDENTIFIER SIGN PER E175 AMM 33-50-15-000/400-801-A. OPS TEST GOOD. RETURNED TO SERVICE.

Source: SDR QXEA2024102100246 · FAA SDRS
J · 2024-07-27 Matched by certificate designator
ATA 3240

EMER/PRKG BRAKE LIGHT ILLUMINATED AFTER BRAKE RELEASE DURING THE PUSH A COUPLE TIMES, BUT THEN WAS NORMAL AFTER SETTING THE BRAKE AFTER THE PUSH, AND AFTER RELEASING THE BRAKE FOR TAKEOFF THRUST, WE GOT A MASTER WARNING "NO TAKEOFF BRAKES", A MASTER CAUTION, AND A CYAN EMER BRAKE FAULT EICAS LIGHT MESSAGE. ABORT WAS AT APPROXIMATELY 40KIAS. ABORTED TAKE OFF. REMOVED FROM SERVICE. INTERROGATED CMC, FOUND FAULT: 3200016UT1 AND 3240005-UT1. PERFORMED FIM 32-41-00-810-864-A ITEM'S 1-7D ON CMC EMER PARK BRK2 PRESS (INBD) STATUS INTERMITTENTLY SWITCHES BETWEEN TRUE AND FALSE WITH EMERGENCY PARKING BRAKE OFF. OUTBD STATUS STAYS CONSTANTLY FALSE. OPENED AND CLOSED PANEL 195AR REMOVED AND REINSTALLED ELECTRICOIL CONNECTOR FOR #2 EMERGENCY PARKING BRAKE PRESSURE SWITCH CLEANED CONNECTOR OAW E175 SWPM 20-61-20 NO HELP. REMOVED & REPLACED #2 EMERGENCY PARKING BRAKE PRESSURE SWITCH IAW E175 AMM TASK 32-44-09-000/400-801-A. OPS TEST GOOD, NO LEAKS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2024072900179 · FAA SDRS
O · 2024-06-12 Matched by certificate designator
ATA 7600

PER ENGINEERING REQUEST TCQ REPLACEMENT REG. REMOVED AND REPLACED THUST CONTROL QUADRANT IAW E175 AMM 76-11-01-000/400-801-A. OPS TEST GOOD. AIRCRAFT STATUS REMAINS CAT III QUALIFIED COCKPIT PLACARD READS CAT III MTX CTRL ADVICED.

Source: SDR QXEA2024061200154 · FAA SDRS
O · 2023-12-24 Matched by certificate designator
ATA 3200

5 DEGREES BANK ON TAXI, LEFT MAIN STRUT COLLAPSE. REMOVED FROM SERVICE. INSPECTED LEFT MAIN LANDING GEAR STRUT IAW 12-12-07-220-801-A, STRUT LOW. SERVICED LH MAIN LANDING GEAR SHOCK STRUT IAW AMM TASK 12-12-07-600-805-A AS PRECAUTION. R+R LH MLG NITROGEN CHARGING VALVE IAW E175 CMM 32-11-01. PERFORMED LH MLG SHOCK STRUT SERVICING IAW E175 AMM 12-12-07-600-801-A. NO OTHER DEFECTS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2023122600189 · FAA SDRS
O · 2023-09-29 Matched by certificate designator
ATA 5320

RH INBD FLOOR SUPPORT CORRODED BETWEEN FRAMES 86-87. REMOVED AND REPLACED RH INBD FLOOR SUPPORT IAW SRM 51-40-08.

Source: SDR QXEA2023100600140 · FAA SDRS
O · 2023-09-25 Matched by certificate designator
ATA 5347

CORROSION LH INBD SEAT TRACK CORRODED AS MARKED AT BACK SIDE OF TEATH AND UNDER PROTECTIVE PLATE. PERFORMED A SPLICE REPAIR FR83-84 REF ETD2023-170-023288 REV A.

Source: SDR QXEA2023092500135 · FAA SDRS
B · 2023-04-21 Matched by certificate designator
ATA 2120

FO AND FA REPORTS SLIGHT ELECTRICAL BURNING SMELL IN COCKPIT AND FWD GALLEY AFTER LANDING. REMOVED FROM SERVICE. NO ABNORMAL ODOR UPON ARRIVAL AT AIRCRAFT. C/W ODOR INSPECTION TASKS 21-20-00-810-801A AND 25-30-00-810-801A. NO DEFECTS NOTED ANYWHERE ON AIRCRAFT. RETURNED TO SERVICE.

Source: SDR QXEA2023042400073 · FAA SDRS
O · 2023-04-02 Matched by certificate designator
ATA 1100

LI DOOR MISSING 5 EMERGENCY REQUIRED PLACARDS, REMOVED FROM SERVICE. INSTALLED 5 EA REQUIRED PLACARDS PER E-175 IPC 11-32-03 &INTRO SECTION TABLE 13. RETURNED TO SERVICE.

Source: SDR QXEA2023040300058 · FAA SDRS
O · 2022-12-28 Matched by certificate designator
ATA 3222

TUG STRAP FOUND HANGING FROM NOSEGEAR SCISSOR ON TAXI IN. REMOVED TOW STRAP FROM GEAR. PERFORMED AN INSPECTION OF NOSE LANDING GEAR AND DOORS AND SURROUNDING AREA IAW AMM 32-20-00-200-801-A. NO DEFECTS NOTED.

Source: SDR QXEA2022123000349 · FAA SDRS
O · 2022-10-01 Matched by certificate designator
ATA 3350

FLIGHT ATTENDANT REPORTS PART OF LIGHTING STRIP MISSING ABEAM ROW 12, #1 SIDE. REMOVED FROM SERVICE. PERFORMED GVI OF PHOTOLUMINESCENT STRIP FOR ROW 12 LH SIDE. FOUND STRIP OVERLAPING. REALIGNED STRIP REF E175 AMM 33-50-21-400-801-A. NO FURTHER DEFECTS NOTED. RETURNED TO SERVICE. NO PARTS REPLACED.

Source: SDR QXEA2022100300299 · FAA SDRS
O · 2022-08-24 Matched by certificate designator
ATA 3200

DURING POST FLIGHT, FOUND SEVERE AMOUNT OF TREAD MISSING FROM R/H INBOARD MAIN TIRE. REMOVED FROM SERVICE. REPAIRED ON WO 322442. REPLACED BOTH RH MLG TIRES AND PERFORMED INSPECTION IAW AMM 05-50-15-200-801A. FOUND #2 ENGINE FIRE EXTINGUISHER DISCHARGE TUBE IAW 20-10-03-400-801A, P/N 170-0897-405. RETURNED TO SERVICE.

Source: SDR QXEA2022082600277 · FAA SDRS
O · 2022-03-17 Matched by certificate designator
ATA 7311

FUEL DRIPPING FROM #1 ENG FUEL PUMP MAIN SEAL DRAIN LINE. REMOVED #1 ENGINE FUEL PUMP REF E175 AMM TASK 73-11-01-000-801-A STEP 1-7 AND GE LMM 73-00-00-800-802 STEPS 1-7, 8 IS N/A AND STEP 9. INSTALLED NEW #1 ENGINE FUEL PUMP REF AMM 73-11-01-400-801-A. OPS AND LEAK CHECKS GOOD.

Source: SDR QXEA2022031800119 · FAA SDRS
B · 2021-10-02 Matched by certificate designator
ATA 3200

RIGHT MAIN OUTER TIRE SMOKING TEMP GREEN 280. REMOVED FROM SERVICE. PERFORMED GVI OF #4 BRAKE ASSEMBLY. NO DEFECTS NOTED. NO EVIDENCE OF FLUID OR FOD BRAKE WAS WARM TO THE TOUCH NOT HOT. FLIGHT DECK TEMP GAGE STAYED IN GREEN. NO OTHER DEFECTS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2021100400463 · FAA SDRS
W · 2021-05-14 Matched by certificate designator
ATA 2897

DURING FQIS HARNESS INSPECTION FOUND INCORRECT ROUTING UNDER PANEL 195AL. CUT ZIPTIES, SEPARATED FQIS FROM ALL OTHER WIRES, SECURED HARNESS IN PANEL 195AL. C/W TC E-28-0007.

Source: SDR QXEA2021062300312 · FAA SDRS
O · 2021-05-05 Matched by certificate designator
ATA 5240

FA REPORTED THAT THE R1 DOOR WAS VERY DIFFICULT TO DISARM. REMOVED FROM SERVICE. INSPECTED GIRT BAR AND ATTACHMENT FITTINGS WITH NO DEFECTS NOTED. VERIFIED R1 DOOR ARMS + DISARMS AS REQUIRED.

Source: SDR QXEA2021050700220 · FAA SDRS
J · 2020-12-22 Matched by certificate designator
ATA 2460

SPDA FAIL MESSAGE CYAN COLOR CRUISE FL 34, RAN QRH RETURNED TO FIELD, LANDING UNEVENTFUL. REMOVED FROM SERVICE.UPON ARRIVAL, THE FOLLOWING FAULT CODE WERE RETRIEVED "SPDA 2- 24610016SP2. C/W E175 FIM 24-61-00-810-810-A. SUSPECT FAILURE OF SPDA 2 MICRO/COM SLOT 8. R & R SPDA 2 MICRO/COM SLOT 8, IAW E175 AMM 24-61-07-00/400-801-A. "SPDA FAIL" MESSAGE NO LONGER DISPLAYED ON EICAS. NO FURTHER DEFECTS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2020122300361 · FAA SDRS
B · 2020-12-20 Matched by certificate designator
ATA 2120

SMELL OF SMOKE REPORTED BY FA'S BETWEEN ROW 12-15 AND IN THE FORWARD GALLEY. REMOVED FROM SERVICE. UPON ARRIVAL TO A/C ELECTRICAL SMELL HAD DISSIPATED. NO MAINTENANCE MESSAGES. C/W E175 FIM TASK 21-20-00-810-803-A. INSPECTED CABIN AND LAV FOR ANY CONTAMINATION, NONE FOUND. INSPECTED COFFEE MAKERS AND OVENS FOR ANY ABNORMALITIES, NONE FOUND. OPERATED PACKS FROM COLD TO FULL HOT AND BACK TO COOL, NO EVIDENCE OF ELECTRICAL SMELLS DURING PACKS OPERATION, REF AMM 21-51-00-710-801-A. ALSO CABIN LIGHTING WAS ON AND NO ODER NOTED FROM THE LIGHTING. ALSO INSPECTED FWD AVIONICS BAY, NO ODOR OR ELECTRICAL SMELLS NOTED. CREW COMPLETED M-744 CHECKLIST, IAW MCN E210016-3, ISS 1. A/C IS OK FOR SERVICE.

Source: SDR QXEA2020122200356 · FAA SDRS
O · 2020-01-07 Matched by certificate designator
ATA 3350

PHOTOLUMINESCENT INDICATOR LIGHT STRIP IN FRONT OF FIRST CLASS SEAT 1ED DOES NOT ILLUM. REPLACED PHOTOLUMINESCENT INDICATOR STRIP IAW E175 AMM 33-50-21-000-801-A AND 33-50-21-400-801-A.

Source: SDR QXEA2020010800013 · FAA SDRS
O · 2019-04-12 Matched by certificate designator
ATA 3350

PHOTOLUMINESCENT STRIP BETWEEN 1A AND 2A NOT ILLUMINATING. PLACED ON MEL 33-50-21A. CLEARED 4/16/19 REPLACED PHOTOLUMINESCENT STRIP IN REF. TO 33-50-21-000/400-801-A. THIS CLEARS MEL. OPS CHECK GOOD. NO OTHER DEFECTS. RETURNED TO SERVICE.

Source: SDR QXEA2019041600179 · FAA SDRS
N · 2019-03-14 Matched by certificate designator
ATA 2621

CREW REPORTS ENG 1 AND ENG 2 FIREX BOTTLE B FAIL ON EICAS. REMOVED FROM SERVICE. C/W FIM TASK 26-21-00-810-810-A00. ENG 1 & ENG 2 FIREX BTL B FAIL MESSAGE EXTINGUISHED. PERFORMED ENGINE FIRE DETECTION LOOP OPERATIONAL CHECK IAW AMM TASK #26-11-00-710-802-A OPERATIONAL TESTED GOOD. MESSAGES REMAINED EXTINGUISHED. NO FURTHER DEFECTS NOTED. RETURNED TO SERVICE. NO PARTS REPLACED.

Source: SDR QXEA2019031500120 · FAA SDRS
J · 2019-01-01 Matched by certificate designator
ATA 2131

BELOW 1000 FT AGL BLEED 1 OVER PRESS MASTER CAUTION EICAS MSG ILLUMINATED CABIN ALT CONT CLIMB EVEN THOUGH (400 FPM) A/C ALT STABILIZED AT 15000. CABIN ALT STABILIZED AT 7300. CREW EXPERIENCED SIGNS OF HYPOXIA. ALSO PACK 1 AND 2 OFF ADU EICAS MESSAGE AND AUTO THROTTLES DISCONNECTED ON CLIMB OUT. RETURNED TO FIELD. LANDING UNEVENTFUL. REMOVED FROM SERVICE. PERFORMED PRESSURIZATION LEAKAGE FUNCTIONAL TEST IAW E-175 AMM TASK 21-31-00-720-802-A. FUNCTIONAL TEST PASS. NO FURTHER DEFECTS NOTED. NO PARTS REPLACED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR QXEA2019010300002 · FAA SDRS
O · 2018-09-01 Matched by certificate designator
ATA 5210

MAIN CABIN DOOR DIFFICULT TO OPEN FROM OUTSIDE. REMOVED FROM SERVICE. OPENED AND CLOSED MCD MULTIPLE TIMES AND FOUND TO BE SLIGHTLY STIFF. LUBED OUTSIDE DOOR MECHANISM. STIFFNESS GONE. OPERATIONS NORMAL. NO FURTHER DEFECTS NOTED. RETURNED TO SERVICE.

Source: SDR QXEA2018090400321 · FAA SDRS