N63978

BEECH C-99 · 1981 · Valid Registration

Registered owner: UAS TRANSERVICES INC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AMERIFLIGHT, LLC (JIKA)Certificate holderMatched by certificate designator
Wiggins Airways, Inc. (AXSA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1993-02-24 Matched by aircraft (N-number)
Beech C-99 None injuryWiggins Airways, Inc.
Source: NTSB case SEA93LA067

Maintenance disclosures

J · 2025-08-21 Matched by certificate designator
ATA 3230

PILOT REPORTED THAT ON FINAL APPROACH HE SELECTED GEAR DOWN AND NOTHING HAPPENED. PILOT CYCLED LANDING GEAR SELECTOR SEVERAL TIMES BEFORE RECEIVING A HYDRAULIC LOW WARNING ANNUNCIATOR. PILOT PULLED THE CIRCUIT BREAKER MANUALLY EXTENDED THE LANDING GEAR THEN LANDED SAFELY. MAINTENANCE TESTED AND FOUND THE LANDING GEAR MOTOR AND RELAY INOPERATIVE. BOTH COMPONENTS WERE REPLACED AND APPROVED AIRCRAFT FOR RETURN TO SERVICE. NO FURTHER SYSTEM FAILURES NOTED ON SUBSEQUENT FLIGHTS.

Source: SDR JIKA202508260001 · FAA SDRS
Z · 2021-12-15 Matched by certificate designator
ATA 3230

THE PILOT WAS COMPLETING A REVENUE FLIGHT FROM MHT TO RUT. HE STATED THAT WHEN APPROACHING RUT HE HAD 3 GREEN LIGHTS BUT THE HYDRAULIC PRESSURE DROPPED, THE LANDING GEAR BREAKER POPPED AND HE DIDN’T FEEL THE GEAR HAD FULLY EXTENDED. HE DID NOT DECLARE AN EMERGENCY. THE PILOT PERFORMED A FLYBY AT RUT AND GROUND MAINTENANCE REPORTED TO HIM THAT THE NOSE GEAR WAS NOT FULLY DOWN. HE USED THE EMERGENCY HAND PUMP TO SUCCESSFULLY COMPLETE THE GEAR EXTENSION. THE PILOT LANDED WITHOUT INCIDENT ON RUNWAY 31 AT RUT. THE AIRCRAFT WAS FERRIED (GEAR DOWN) TO ITS MAINTENANCE BASE AT MHT THE SAME DAY, WHERE THE LANDING GEAR HYDRAULIC POWER PACK MOTOR WAS CHANGED AND THE AIRCRAFT PLACED BACK IN SERVICE. THE FAILED MOTOR WAS INSTALLED ON 10/28/2020 AND HAD 323.2 HRS AND 431 LANDINGS SINCE OVERHAUL. OVERHAUL IS DUE AT 10,000 LANDINGS.

Source: SDR 2021F00348 · FAA SDRS
Z · 2021-12-15 Matched by certificate designator
ATA 3230

THE PILOT WAS COMPLETING A REVENUE FLIGHT FROM MHT TO RUT. HE STATED THAT WHEN APPROACHING RUT HE HAD 3 GREEN LIGHTS BUT THE HYDRAULIC PRESSURE DROPPED, THE LANDING GEAR BREAKER POPPED AND HE DIDN’T FEEL THE GEAR HAD FULLY EXTENDED. HE DID NOT DECLARE AN EMERGENCY. THE PILOT PERFORMED A FLYBY AT RUT AND GROUND MAINTENANCE REPORTED TO HIM THAT THE NOSE GEAR WAS NOT FULLY DOWN. HE USED THE EMERGENCY HAND PUMP TO SUCCESSFULLY COMPLETE THE GEAR EXTENSION. THE PILOT LANDED WITHOUT INCIDENT ON RUNWAY 31 AT RUT. THE AIRCRAFT WAS FERRIED (GEAR DOWN) TO ITS MAINTENANCE BASE AT MHT THE SAME DAY, WHERE THE LANDING GEAR HYDRAULIC POWER PACK MOTOR WAS CHANGED AND THE AIRCRAFT PLACED BACK IN SERVICE. THE FAILED MOTOR WAS INSTALLED ON 10/28/2020 AND HAD 323.2 HRS AND 431 LANDINGS SINCE OVERHAUL. OVERHAUL IS DUE AT 10,000 LANDINGS.

Source: SDR 2021F00349 · FAA SDRS
O · 2016-11-12 Matched by certificate designator
ATA 7200

DURING A SCHEDULED BOROSCOPE OF THE RT ENGINE, THE COMPRESSOR TURBINE BLADES WERE FOUND DAMAGED BY FOD AND A POWER TURBINE CONTAINMENT SHROUD BOLT HEAD WAS FOUND BROKEN OFF AND RETAINED BY SAFETY WIRE. THE REST OF THE BOLT BACKED OUT OF ITS THREADED HOLE AND PASSED THROUGH THE COMPRESSOR TURBINE STATOR & DISC AND THE POWER TURBINE STATOR & DISC BEFORE EXITING THE ENGINE.

Source: SDR AXSA2019112800001 · FAA SDRS
C · 2016-11-12 Matched by certificate designator
ATA 7250

DURING A SCHEDULED BORESCOPE OF THE RT ENGINE FOUND THE CT BLADES WERE FOUND TO BE DAMAGED DUE TO FOD. A POWER TURBINE CONTAINMENT SHROUD BOLT HEAD WAS FOUND BROKEN OFF AND STILL TIED WITH SAFETY WIRE. THE REMAINDER OF THE BOLT HAD VIBRATED OUT OF ITS HOLE AND CAUSED FOD DAMAGE BEFORE EXITING THE SPACE.

Source: SDR 2017F00176 · FAA SDRS
J · 2015-04-07 Matched by certificate designator
ATA 3233

ON APPROACH, THE PILOT SELECTED THE LG TO THE DOWN POSITION. THE LG FAILED TO EXTEND & THE LG CONTROL CB POPPED. THE PILOT RESET THE CB & CYCLED THE LG WITH THE SAME RESULTS, THE CB POPPED & THE LG WOULD NOT EXTEND. THE PILOT PERFORMED AN EMER GEAR EXTENSION, THE LG EXTENDED TO THE FULL DOWN & LOCKED POSITION WITH 3 GREEN SAFE INDICATIONS. THE PILOT LANDED WITHOUT INCIDENT. MX FOUND THE LG ELEC MOTOR, PN 115-380002-5 INOPERATIVE. R & R THE LG MOTOR. THE LANDING SYS WAS FUNCTIONAL CHECKED THROUGH FIVE GEAR CYCLES. LG SYS CHECKED NORMAL..

Source: SDR JIKA2015040701 · FAA SDRS
K J · 2014-06-17 Matched by certificate designator
ATA 2910

AFTER DEPARTURE PILOT SELECTED LG HANDLE TO RETRACT POSITION, LG FAILED TO FULLY RETRACT. PILOT TROUBLESHOOTING REVEALED CB HAD POPPED & LG RED INDICATOR LIGHT WAS ILLUMINATED. RESET CB & PLACED LG HANDLE IN EXTEND POSITION, BOTH LT & RT MLG EXTENDED & LOCKED, NOSE GEAR FAILED TO EXTEND, CB POPPED AGAIN & LOW HYD FLUID INDICATOR LIGHT ILLUMINATED. PILOT DECIDED TO MANUALLY EXTENDED LG USING EMER PROCEDURES & LANDED WITHOUT FURTHER INCIDENT. INSPECTION OF ACFT FOUND THE HYD LINE CONNECTED TO 20619-1 FITTING WAS CRACKED. R & R FITTING IAW MM 29-10-00, PERFORMED LG OPERATIONAL CHECKS IAW MM 32-31-00. ALL OPERATIONAL CHECKS WERE NORMAL.

Source: SDR JIKA2014061701 · FAA SDRS