N639DS

AGUSTA AEROSPACE CORP AW139 · 2011 · Valid Registration

Registered owner: CHEVRON USA INC, MS (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CHEVRON USA PRODUCTION COMPANY (AC2A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-10-30 Matched by certificate designator
ATA 2910

#2 PCM (HYDRAULIC POWER CONTROL MODULE) LEAKING AT CRACK IN BOSS CASTING.

Source: SDR AC2A2022103113901 · FAA SDRS
O · 2022-05-25 Matched by certificate designator
ATA 5330

R/H LONGERON AT STA5700 HAS CRACK COMING FROM RIVET TO CORNER WEBBING. CORRECTIVE ACTION - REMOVED LOWER 3 ANGLES CUT DAMAGED WEBBING (WALL) . CUT ACCESS PANEL INTO FRONT OF THE DRY BAY REMOVED WALL . FABRICATED INBOARD AND OUTBOARD DOUBLER FOR SPLICE REPAIR OF NEW WALL SECTION. BACK DRILLED NEW WALL SECTION AND LOCATED DOUBLERS. RENO01 5/29/2022. BACKDRILLED REMAINING ANGLES AND INSTALLED WEB, DOUBLERS, AND ANGLES IN REF TO AGUSTA AW139 39A53-33-08-01A-664A-D. SEE TASK# 87, 105, 106, 107, 108 FOR REFERENCE.

Source: SDR AC2A2022060813901 · FAA SDRS
O · 2022-05-25 Matched by certificate designator
ATA 5302

TAIL STRUCTURE DELAMINATED INSIDE AND OUTSIDE AT R/H STA11020 UPPER AREA. CORRECTIVE ACTION - CARRIED FORWARD TO CRS AC2R685K SHEETMETAL SHOP W/O TASK C06456-1 FOR CORRECTIVE ACTION.

Source: SDR AC2A2022060813902 · FAA SDRS
O · 2021-07-21 Matched by certificate designator
ATA 6321

ROTOR BRAKE CAS FAIL MESSAGE ILLUMINATED ON SHUTDOWN, ACTUATOR STUCK IN UP POSITION.

Source: SDR AC2A2021072213901 · FAA SDRS
K · 2021-04-03 Matched by certificate designator
ATA 3240

PARKING BRAKE PRESSURE SWITCH LEAKING AT VENT HOLE

Source: SDR AC2A2021040413901 · FAA SDRS
O · 2020-11-13 Matched by certificate designator
ATA 6321

ROTOR BRAKE WILL NOT BUILD PRESSURE. ROTOR BRAKE CONTROL MODULE WAS FOUND TO BE DEFECTIVE. MODULE WAS PREVIOUSLY REPAIRED BY MANUFACTURE AND BECAME DEFECTIVE IN 379.9 HOURS OF OPERATION.

Source: SDR AC2A2020111413901 · FAA SDRS
O · 2019-05-15 Matched by certificate designator
ATA 5346

CORROSION DAMAGE ON RIGHT OUTBOARD ENGINE MOUNT AIRFRAME SUPPORT FITTING REQUIRING REPLACEMENT OF FITTING.

Source: SDR AC2A2019051513901 · FAA SDRS
O · 2019-04-28 Matched by certificate designator
ATA 7100

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113921 · FAA SDRS
O · 2019-04-28 Matched by certificate designator
ATA 7160

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113913 · FAA SDRS
O · 2019-04-28 Matched by certificate designator
ATA 7160

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113920 · FAA SDRS
O · 2019-04-28 Matched by certificate designator
ATA 7160

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113912 · FAA SDRS
J · 2011-08-29 Matched by certificate designator
ATA 2910

SHORTLY AFTER DEPARTURE, "1 HYD MIN" AND "EMER LDG PRESS" ILLUMINATED. REFERENCED THE SYNOPTIC PAGE AND STARTED THE RETURN TRIP. APPROX 90 SECONDS LATER, "1 HYD OIL PRESS", "1 SERVO" AND "1 HYD PUMP" ILLUMINATED.

Source: SDR AC2A9DS08292011 · FAA SDRS