N639MM

AGUSTA AEROSPACE CORP AW139 · 2009 · Valid Registration

Registered owner: CHEVRON USA INC, MS (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CHEVRON USA PRODUCTION COMPANY (AC2A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2023-06-18 Matched by certificate designator
ATA 6320

ROTOR BRAKE FAIL CAS ILLUMINATED ON SHUT DOWN WITH CALIPER INDICATING DOWN POSITION. REPLACED ROTOR BRAKE ACTUATOR.

Source: SDR AC2A2023062213901 · FAA SDRS
O · 2022-10-30 Matched by certificate designator
ATA 5302

TAIL STRUCTURE HAS AREA OF DELAMINATION ON R/H SIDE.

Source: SDR AC2A2022103013901 · FAA SDRS
O · 2022-03-17 Matched by certificate designator
ATA 5300

CORROSION DAMAGE CAUSING REPLACEMENT OF AFT RIGHT UPPER PLATE.

Source: SDR AC2A2022031713901 · FAA SDRS
O · 2022-01-08 Matched by certificate designator
ATA 7530

DURING TROUBLESHOOTING OF LOW POWER ON #1 ENGINE, #2 ENGINE BLEED VALVE WAS REMOVED TO SWAP WITH #1 ENGINE BLEED VALVE AND FOUND #2 BLEED VALVE SEALING DISC WAS CRACKED. BLEED VALVE WAS REPLACED.

Source: SDR AC2A2022010913901 · FAA SDRS
O · 2021-08-21 Matched by certificate designator
ATA 2700

1 R AP FAIL CAS LIGHT ILLUMINATED DURING CHECK. REPLACED NO 1 ROLL ACTUATOR AND PERFORMED FUNCTIONAL CHECK.

Source: SDR AC2A2021082313901 · FAA SDRS
O · 2021-08-09 Matched by certificate designator
ATA 6320

MGB L/H SUMP CHIP DETECTOR RETAINING GROOVES WORN BEYOND ACCEPTABLE PUBLISHED MANUFACTURE LIMITS AS RECEIVED FROM OVERHAUL CONDITION.

Source: SDR AC2A2021081813901 · FAA SDRS
O · 2020-02-07 Matched by certificate designator
ATA 6520

THE INTERMEDIATE GEARBOX (IGB) CHIP DETECTOR HAS ROTATIONAL MOVEMENT AT THE PIN FOLLOWER RETAINING RING COLLAR.

Source: SDR AC2A2020020713901 · FAA SDRS
O · 2020-01-31 Matched by certificate designator
ATA 7100

IBF MAINTENANCE INDICATOR FOUND CRACKED. *SUPPLEMENTAL INFORMATION* PART NUMBER ENTERED ON ORIGINAL SDR IN SECTION 5 WAS IN ERROR. PART NUMBER WAS SUBMITTED AS 104440-201 AND SHOULD HAVE BEEN 104441-201. *SUPPLEMENTAL INFORMATION* THE UNIQUE CONTROL CODE WAS ALSO ENTERED IN ERROR. UNIQUE CONTROL CODE WAS SUBMITTED AS AC2A202050119 AND SHOULD HAVE READ AC2A2020050113919.

Source: SDR AC2A2020050113919 · FAA SDRS
O · 2018-11-29 Matched by certificate designator
ATA 5210

COCKPIT DOOR OPENED IN FLIGHT. LANDED AT GC205 (NEAREST CHEVRON PLATFORM. AFTER LANDING, CREW INSPECTED AND SECURED DOOR. DETERMINED CAUSE OF DOOR OPENING WAS VIBRATION OF THE DOOR HANDLE.

Source: SDR AC2R2018112901 · FAA SDRS
O · 2018-11-06 Matched by certificate designator
ATA 7160

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113909 · FAA SDRS
O · 2018-10-18 Matched by certificate designator
ATA 7160

IBF MAINTENANCE AID FOUND TO BE CRACKED.

Source: SDR AC2A2020050113908 · FAA SDRS
M B · 2018-03-30 Matched by certificate designator
ATA 2121

PRIOR TO CRUISE CLEARANCE, PILOTS NOTICED A STRONG ELECTRICAL OVERHEAT ODOR WITH A SIMULTANEOUS FWD FAN CAS MESSAGE. NO SMOKE OR FLAMES WERE NOTED. CREW COMPLIED WITH QRH. REPLACED THE PILOT'S COCKPIT FAN.

Source: SDR AC2R2018040201 · FAA SDRS
O · 2017-07-31 Matched by certificate designator
ATA 6410

TAIL ROTOR BLADE CRACK AT INBOARD ROOT NEAR EROSION SHIELD.

Source: SDR AC2R2017073101 · FAA SDRS
O · 2017-07-31 Matched by certificate designator
ATA 6410

TAIL ROTOR BLADE CRACK AT INBOARD ROOT NEAR EROSION SHIELD.

Source: SDR AC2R2017073102 · FAA SDRS
E · 2015-10-31 Matched by certificate designator
ATA 6320

OIL COOLER FAN HIGH VIBRATION READINGS.

Source: SDR AC2R2018042004 · FAA SDRS
N · 2013-09-16 Matched by certificate designator
ATA 7712

ENGINE TORQUE MISCOMPARE CAS MESSAGE ILLUMINATED DURING GROUND RUN. FOUND TORQUE SENSORS DAMAGED FROM CONTACT WITH ROTATING COMPONENT.

Source: SDR AC2A201309170001 · FAA SDRS