N6470H

CESSNA 207A · 1979 · Valid Registration

Registered owner: JB AIRCRAFT LLC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
SNUG CORNER COVE SERVICES LLC (S2TC)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 2007-01-07 Matched by aircraft (N-number)
Cessna 207 None injurySNUG CORNER COVE SERVICES LLC
Source: NTSB case ANC07LA014
Accident · 1994-02-08 Matched by aircraft (N-number)
Cessna 207 None injurySNUG CORNER COVE SERVICES LLC
Source: NTSB case ANC94LA031
Accident · 1988-09-09 Unresolved
Cessna 207 None injuryoperator not yet resolved
Source: NTSB case ANC88LA136
Incident · 1983-03-28 Unresolved
Cessna C-207A None injuryoperator not yet resolved
Source: NTSB case ANC83IA060

Maintenance disclosures

O · 2015-04-07 Matched by certificate designator
ATA 8530

DURING 100HR INSPECTION BORESCOPING ENG, FOUND NR 4 CYLINDER CRACKED FROM LOWER SPARKPLUG BOSS TO EXHAUST VLV SEAT.

Source: SDR YAAA20150407008 · FAA SDRS
O · 2015-04-07 Matched by certificate designator
ATA 8530

DURING 100HR INSPECTION BORESCOPING ENG, FOUND NR 3 CYLINDER CRACKED FROM SPARKPLUG BOSS TO EXHAUST VLV SEAT & VLV TO VLV.

Source: SDR YAAA20150407010 · FAA SDRS
O · 2015-04-07 Matched by certificate designator
ATA 8530

DURING 100HR INSPECTION BORESCOPING ENG, FOUND NR 1 CYLINDER CRACKED FROM LOWER SPARKPLUG BOSS TO EXHAUST VLV SEAT.

Source: SDR YAAA20150407009 · FAA SDRS
O · 2015-03-14 Matched by certificate designator
ATA 8530

DURING 100 HR INSPECTION BORESCOPING ENG, FOUND NR 2 CYLINDER CRACKED FROM LOWER SPARK PLUG BOSS APPROX 1/2 INCH TOWARDS EXHAUST VLV SEAT.

Source: SDR YAAA20150314003 · FAA SDRS
B · 2011-08-04 Matched by certificate designator
ATA 2120

DURING TAKEOFF, SMELL OF SOLVENT, FUMES IN COCKPIT. SUSPECT RESIDUAL SOLVENT/OIL FROM RECENT ENGINE WAS TO BE THE CAUSE OF PROBLEM.

Source: SDR YAA2011F00000 · FAA SDRS
O · 2010-07-02 Matched by certificate designator
ATA 8530

UPON ENGINE DISMANTLE FOR O/H, 5 OUT OF 6 CYLINDERS HAD CRACKED CYLINDER HEADS. THE CRACKS ORIGINATED AT THE LOWER SPARK PLUG HOLE AND RADIATED OUT A THE 4 O`CLOCK POSITION FOR APPROX 1 INCH. AFFECTED SN: 4/ 526-A08-6893. NOTE: THIS INFO WAS SUBMITTED BY AN UNKNOWN PERSON TO THE AL03 FSDO. NO OTHER INFO AVAILABLE.

Source: SDR 2010FA0000791 · FAA SDRS
O · 2010-07-02 Matched by certificate designator
ATA 8530

UPON ENGINE DISMANTLE OR OVERHAUL, 5 OUT OF 6 CYLINDERS HAD CRACKED CYLINDER HEADS. THE CRACKS ORIGINATED AT THE LOWER SPARK PLUG HOLE AND RADIATED OUT AT THE 4 O`CLOCK POSITION FOR APPROX 1 INCH. AFFECTED SN: NR 3- 526-A08-6894. NOTE: THIS INFO WAS SUBMITTED BY AN UNKNOWN PERSON TO THE FSDO. NO OTHER INFO AVAILABLE.

Source: SDR 2010FA0000789 · FAA SDRS
O · 2010-07-02 Matched by certificate designator
ATA 8530

UPON ENGINE DISMANTLE OR OVERHAUL, 5 OUT OF 6 CYLINDERS HAD CRACKED CYLINDER HEADS. THE CRACKS ORIGINATED AT THE LOWER SPARK PLUG HOLE AND RADIATED OUT AT THE 4 O`CLOCK POSITION FOR APPROX 1 INCH. AFFECTED SN: NR 5/ 526-A08-686889. NOTE: THIS INFO WAS SUBMITTED BY AN UNKNOWN PERSON TO THE FSDO. NO OTHER INFO AVAILABLE.

Source: SDR 2010FA0000792 · FAA SDRS
O · 2010-07-02 Matched by certificate designator
ATA 8530

UPON ENGINE DISMANTLE OR OVERHAUL, 5 OUT OF 6 CYLINDERS HAD CRACKED CYLINDER HEADS. THE CRACKS ORIGINATED AT THE LOWER SPARK PLUG HOLE AND RADIATED OUT AT THE 4 O`CLOCK POSITION FOR APPROX 1 INCH. AFFECTED SN: NR 2- 526-A08-6901. NOTE: THIS INFO WAS SUBMITTED BY AN UNKNOWN PERSON TO THE FSDO. NO OTHER INFO AVAILABLE.

Source: SDR 2010FA0000788 · FAA SDRS
O · 2010-07-02 Matched by certificate designator
ATA 8530

UPON ENGINE DISMANTLE OR OVERHAUL, 5 OUT OF 6 CYLINDERS HAD CRACKED CYLINDER HEADS. THE CRACKS ORIGINATED AT THE LOWER SPARK PLUG HOLE AND RADIATED OUT AT THE 4 O`CLOCK POSITION FOR APPROX 1 INCH. AFFECTED SN: NR 1- 526-A08-6899. NOTE: THIS INFO WAS SUBMITTED BY AN UNKNOWN PERSON TO THE FSDO. NO OTHER INFO AVAILABLE.

Source: SDR 2010FA0000787 · FAA SDRS
O · 2010-05-28 Matched by certificate designator
ATA 7310

FUEL SUPPLY HOSE FITTING AT FLOW DIVIDER LOOSENED.

Source: SDR YAA2010F00001 · FAA SDRS
B · 2008-11-05 Matched by certificate designator
ATA 7810

PILOT REPORTED SMOKE IN COCKPIT AFTER TAKEOFF, HE LANDED ACFT SAFELY AND TAXIED TO MAINT HANGER. MAINT FOUND HOLE AND CRACK IN EXHAUST NEAR HEATER MUFFLER. REMOVED AND REPLACED LT EXHAUST COLLECTOR, RAN UP ENGINE, FOUND OK FOR SERVICE ALL AD`S ON EXHAUST ARE CURRENT, NORMAL EXHAUST FAILURE THAT WOULD HAVE BEEN CAUGHT AT NEXT 100 HR INSP. ACFT WAS 30 HRS AWAY FROM NEXT 100 HR. (K)

Source: SDR YAA2008F00000 · FAA SDRS