N650HJ

BOMBARDIER INC CL-600-2B16 · 2006 · Valid Registration

Registered owner: LAMBRO AIRCRAFT MANAGEMENT LLC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ACE AVIATION SERVICES CORPORATION (V6NA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-08-11 Matched by certificate designator
ATA 5347

AT SCHEDULE INSPECTION, DISCOVERED SEAT RAIL UNDER LAVATORY TOILET CORRODED. REPLACED FLOOR RAIL WITH NEW.

Source: SDR V6NA2022081101 · FAA SDRS
O · 2021-08-18 Matched by certificate designator
ATA 5347

AT SCHEDULED INSPECTION, DISCOVERED CORROSION ON SEAT RAIL BEAM UPPER SURFACE, FS574.00 TO 605.00, WL73.5. CORROSION WAS REMOVED. DOUBLER REPAIR ANGLES OF 0.063 IN. 2024-T3 WERE INSTALLED WET USING MS20426AD RIVETS AND HL18PB5 HILOKS. REPAIR PERFORMED PER FAA APPROVED DATA IN DRAWING HAJ-GEBD604-5653-M04, REV. I/R FROM FAA DER DERT-605388-NM.

Source: SDR V6NA202109021801 · FAA SDRS
O · 2021-08-18 Matched by certificate designator
ATA 5347

AT SCHEDULED INSPECTION, DISCOVERED CORROSION ON SEAT RAIL BEAM UPPER SURFACE, FS574.00 TO 605.00, WL73.5. CORROSION WAS REMOVED. DOUBLER REPAIR ANGLES OF 0.063 IN. 2024-T3 WERE INSTALLED WET USING MS20426AD RIVETS AND HL18PB5 HILOKS. REPAIR PERFORMED PER FAA APPROVED DATA IN DRAWING HAJ-GEBD604-5653-M04, REV. I/R FROM FAA DER DERT-605388-NM.

Source: SDR V6NA202109028011 · FAA SDRS
O · 2020-12-03 Matched by certificate designator
ATA 5330

AT SCHEDULED INSPECTION, DISCOVERED DENT IN FUSELAGE BELLY SKIN AT FS 646 FRAME 640, TEN INCHES FROM CENTER. DAMAGE DIMENSIONS APPROXIMATELY 3.0 X 8.3. FASTENERS WERE REMOVED IN AREA, SKIN AND STRAP MECHANICALLY FORMED BACK TO ORIGINAL CONTOUR. REFORMED AREA VERIFIED NOT TO BE CRACKED, PER EDDY CURRENT INSPECTION METHOD. BENT SECTION OF FRAME 640 WAS REMOVED, FILLER WAS INSTALLED SANDWICHED BETWEEN TWO REINFORCEMENT DOUBLERS. DOUBLER REPAIR EXTENDING FIVE ROWS OF RIVETS BEYOND SEAM WAS PERFORMED PER STRUCTURAL REPAIR MANUAL 51-70-12, FIGURE 2, SHEET 2.

Source: SDR V6NA20201206001 · FAA SDRS
O · 2019-12-04 Matched by certificate designator
ATA 3220

AT SCHEDULED INSPECTION DETERMINED NOSE LANDING GEAR UPPER TORQUE LING ATTACHMENT TO LOWER TORQUE LING CASTELLATED NUT MIGRATING OUTWARD OFF OF TORQUE LINK APEX PIN DUE TO SECURING PIN MISSING. INSPECTED OPPOSITE PIN AND DETERMINED EXISTING PIN TO BE WORN. NO DAMAGE TO APEX PIN OR NUT. REPLACED EXISTING PIN AND MISSING PIN WITH NEW.

Source: SDR V6NA20191209401 · FAA SDRS
O · 2018-08-20 Matched by certificate designator
ATA 5310

PASSENGER DOOR AFT FRAME AT BS 349, THE DOOR POWER ASSIST CABLE MOUNT WAS CORRODED. CABLE MOUNT WAS REPAIRED IAW DRAWING HAJ-GEBD604-5653-M01-1.

Source: SDR V6NA2018082002 · FAA SDRS