N651BC

SAAB-FAIRCHILD 340A · Valid Registration

Registered owner: AVIATION INVENTORY RESOURCES INC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
IBC AIRWAYS, INC. (OZCA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-11-03 Matched by certificate designator
ATA 7930

DURING CRUISE FLIGHT AT 17000 FT LEFT ENGINE CHIP DETECT LIGHT ILLUMINATED A8-15 QRH. NO OTHER ABNORMALITIES. -- REMOVED AND REPLACED LT HAND ENGINE CHIP DETECTOR I/AW GE-CT-5 AMM 79-30-35-04. RUN AND LEAKS CHECK SATISFACTORY

Source: SDR OZCA340076221103 · FAA SDRS
O · 2022-01-28 Matched by certificate designator
ATA 7297

WHILE INCRISING POWER LEVERS AT START OF T/O ROLL, L ENGINE TORQUE UNCOMANDED TO 120% ( RED LIGHT ON ) REDUCED POWER LEVER, ENGINE DID NOT RESPOND. SHUT ENGINE DOWN. ASYMETRIC THRUST FROM RUNNING RIGHT ENGINE QUICKLY CAUSED PLANE TO ROTATE TO THE LEFT. RIGHT ENGINE WAS SHUT DOWN. - REPLACED AUTOCOARSEN COMPUTER, CHECKED OUT WIRING FOR 64 DEG SWITCH TO RELAYS 43KA AND 44KA AND TO THE CTOT PANEL CHECKED GOOD. FOUND THE BOTTOM GEVERNOR PREMATURELY ENGAGING REPLACED HMU AND OPS CHECK NORMAL. AFTER A SUCCESSFUL FCF WITHOUT REPEATING THE FAULT, WE DECIDED TO CHANGE THE ENGINE HARNESS AS A PRECAUTION.

Source: SDR OZCA340076220128 · FAA SDRS
B · 2020-11-16 Matched by certificate designator
ATA 2120

CREW REPORTED, ATOMIZED OIL HAZE IN COCKPIT UNABLE TO SEE OUTSIDE OF INSTRUMENTS, AFTER HP'S WERE TURNED ON AND RECIRCLE SWITCH. MAINTENANCE PERFORMED, INSPECTED LT AND RT ACM'S FOR LEAKS AND OPERATIONS CHECK. INSPECTED LT AND RT ENGINE FOR INTERNAL OIL LEAKS, NO FAULTS FOUND. PERFORMED LT AND RT ENGINE RUN, IAW SAAB 340 72-00-00, NO FAULTS FOUND.

Source: SDR OZCA202011190001 · FAA SDRS
J · 2015-08-31 Matched by certificate designator
ATA 7922

ABOUT 10 MINUTES AFTER TAKEOFF, RT ENG OIL TEMP WENT ABOVE RED LINE. REDUCED POWER & FOLLOWED QRH. TEMP SLOWLY STARTED TO REDUCE, OIL PRESS WAS 48 PSI. TROUBLE SHOT SYS & FOUND COLD OIL RELIEF VLV INOPERATIVE. R & R RT COLD OIL RELIEF VLV. GND OPERATIONAL CHECKED SATISFACTORY & CHECK FLIGHT ALSO SATISFACTORY.

Source: SDR OZCA20150831018 · FAA SDRS
R · 2014-09-19 Matched by certificate designator
ATA 7600

DURING FLIGHT CREW EXPERIENCED A LOSS OF THE NR 2 PROPELLER RPM. ACFT RETURNED BACK TO AIRPORT & LANDED SAFELY. INSPECTED THE ACFT & FOUND THE RT WING TO NACELLE CONTROL CABLE AT FAULT. AFFECTED CABLE WAS REPLACED. RIGGING CHECKS WERE SATISFACTORY & ENG RUNS WERE SATISFACTORY.

Source: SDR OZCA20140922001 · FAA SDRS
N · 2014-03-27 Matched by certificate designator
ATA 2612

RIGHT ENGINE FIRE WARNING, RETURNED TO AIRPORT. REPLACED RT FIRE DETECTOR CONTROL BOX WITH AN INSPECTED PART & ACFT WAS RELEASED TO SERVICE.

Source: SDR OZCA20140327001 · FAA SDRS