N662AR

LEARJET INC 60 · 2001 · Valid Registration

Registered owner: JET SALES EAST LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ATI JET INC. (G41A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2026-01-24 Matched by certificate designator
ATA 7931

ON 1/24/2026 N662AR, CYO662 WAS DEPARTING KSUA HEADING TO KNAS. DURING CLIMB, THE CAPTAIN NOTICED THE LH ENGINE OIL PRESSURE WAS FLUCTUATING. THE SCHEDULED FLIGHT WAS OVER WATER SO THE CAPTAIN ELECTED TO RETURN TO KSUA. LOCAL MAINTENANCE WAS CALLED TO INVESTIGATE THE ISSUE. ENGINE OIL LEVELS WERE CHECKED AND FOUND TO BE NORMAL. ENGINE RUNS COMPLETED WITH ALL INDICATIONS NORMAL. THE MECHANIC THEN SWAPPED OIL PRESSURE TRANSMITTERS AND RAN ENGINES AGAIN. ALL INDICATIONS WERE NORMAL. THE LH ENGINE OIL PRESSURE/TEMPERATURE INDICATOR WAS REPLACED AND ENGINE RUNS COMPLETED. ALL INDICATIONS FOUND TO BE NORMAL - NO DEFINITIVE CAUSE OF FLUCTUATION COULD BE FOUND. AIRCRAFT WAS RETURNED TO SERVICE AND HAS BEEN ON SEVEN FLIGHTS SINCE WITH NO OTHER ISSUES REPORTED.

Source: SDR 2026F00006 · FAA SDRS
O · 2023-04-18 Matched by certificate designator
ATA 3240

ON 4/15/23, N662AR FLEW FROM KVNY TO KLAS. AS THE CREW COMPLETED A NORMAL LANDING OF THE AIRCRAFT IN LAS, THEY WERE INSTRUCTED TO TURN OFF ON A HIGH SPEED TAXI WAY AND PROCEED TO PARKING. THE TRS WERE DEPLOYED AND WORKING NORMALLY. AS THE TURN WAS INITIATED AND TRS STOWED THE CREW REPORTED THE STEERING DID NOT RESPOND AND THE BRAKES HAD LITTLE TO NO PEDAL FEEL WHEN PRESSED. THEY WERE COMING UP ON ANOTHER AIRCRAFT THAT WAS AHEAD OF THEM AND ELECTED TO USE THE EMERGENCY BRAKING (EMER AIR) WHICH SLOWED THE AIRCRAFT WHILE THE AIRCRAFT IN FRONT WAS ABLE TO MOVE ON AND WAS CLEAR. WITH ENOUGH RAMP SPACE AND NO OTHER AIRCRAFT NEARBY, THE AIRCRAFT WAS SLOWING ON ITS OWN INTO A LH TURN, THE CAPTAIN LET IT CONTINUE ON THE TURN WHICH SLOWED THE AIRCRAFT ALMOST TO A STOP. HE THEN CAME TO A COMPLETE STOP WITH A SMALL INPUT OF EMER AIR. HE THEN FELT SOLID BRAKE PRESSURE RESISTANCE ON THE BRAKE PEDALS AND THE STEERING STARTED WORKING AGAIN. THE AIRCRAFT WAS PARKED AT THE FBO WITH STEERING AND BRAKING ACTION WORKING NORMALLY. ON 4/17 ATI JET MAINTENANCE WAS DISPATCHED TO LAS TO INSPECT THE AIRCRAFT. NO DISCREPANCIES WERE FOUND. BRAKING WAS NORMAL, STEERING SYSTEM ALSO FOUND TO BE WORKING NORMALLY. A FERRY PERMIT WAS GRANTED AND A NORMAL TAXI/TAKEOFF DEPARTING LAS WITH THE SAME IN ELP. NO DETERMINATION HAS BEEN MADE AS TO WHAT CAUSED THE ISSUES IN LAS. ALL ANTI SKID COMPONENTS WILL BE TESTED/INSPECTED AS WELL AS THE STEERING SYSTEM COMPUTER, SERVO AND OTHER RELATED ITEMS.

Source: SDR 2023FA0000221 · FAA SDRS