N665AS

EMBRAER-EMPRESA BRASILEIRA DE EMB-500 · 2009 · Valid Registration

Registered owner: JSSI PARTS LLC, IL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EXECUTIVE FLIGHT SERVICES, LLC (E07A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-07-07 Matched by certificate designator
ATA 7532

BLEED 1 FAIL IN FLIGHT

Source: SDR XMXR2022083005 · FAA SDRS
J · 2021-04-14 Matched by certificate designator
ATA 2782

FLAP FAIL MESSAGE YELLOW BOX ON FLAP INDICATOR ON POWER UP.

Source: SDR XMXR202104230006 · FAA SDRS
E J · 2018-07-09 Matched by certificate designator
ATA 2435

DURING CLIMB OUT CREW NOTICED VIBRATION COMING FROM LT ENGINE. CREW ELECTED TO SHUT DOWN LT ENGINE AND RETURN TO DEPARTURE AIRPORT.

Source: SDR E07A2018071000001 · FAA SDRS
K · 2018-02-07 Matched by certificate designator
ATA 3243

AFTER BRAKE RELEASE. PARK BRAKE LIGHT STAYS ON OR IS INTERMITTENT COMING ON. DURING BRAKE SET. PUMP IS CYCLING EXCESSIVELY.

Source: SDR E07A201802120001 · FAA SDRS
K · 2017-05-16 Matched by certificate designator
ATA 3243

AFTER BRAKE RELEASE. PARK BRAKE LIGHT STAYS ON OR IS INTERMITTENT COMING ON. DURING BRAKE SET. PUMP IS CYCLING EXCESSIVELY.

Source: SDR E07A201802120002 · FAA SDRS
B · 2015-12-03 Matched by certificate designator
ATA 2160

AFTER TAKEOFF, CREW NOTED HOT SMELL & A SMALL BIT OF SMOKE IN THE CABIN. TURNED OFF RT BLEED VLV, SMOKE & HOT SMELL DISSIPATED. DETERMINED RT CABIN TEMP MODULATING VLV WAS STUCK OPEN. INSTALLED NEW VLV, GND RUN & OPERATIONS CHECK WERE SATISFACTORY. ACFT WAS RETURNED TO SERVICE.

Source: SDR E07A20151207001 · FAA SDRS
J · 2014-12-05 Matched by certificate designator
ATA 2913

AFTER TAKEOFF, LANDING GEAR WOULD NOT RETRACT FOLLOWED BY LOW HYDRAULIC CAS MESSAGE.

Source: SDR 2014FA0000715 · FAA SDRS
B · 2012-05-20 Matched by certificate designator
ATA 3610

ON CLIMBOUT, CREW SMELLED BURNED OIL AND OBSERVED LIGHT SMOKE IN THE AFT CABIN. LECTED TO RETURN FOR INSPECTION. SMOKE AND ODOR DISSIPATED WITHIN MINUTES. AFTER INSPECTION OF ACFT, DETERMINED ODOR AND SMOKE TO HAVE ORIGINATED FROM SMALL AMOUNT OF ENGINE OIL THAT ACCUMULATED IN BLEED AIR SYS DURING ENGINE REMOVAL AND INSTALLATION. IT WAS DETERMINED NO PARTS OR COMPONENTS WERE DEFECTIVE.

Source: SDR E07A20120521512 · FAA SDRS