N67886

CESSNA 402C · 1980 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC DBA, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2021-05-19 Matched by certificate designator
ATA 3243

THE PILOT A LOSS OF PRESSURE ON THE RIGHT BRAKE DURING PARKING. MAINTENANCE INSPECTED AND FOUND THE RIGHT MASTER CYLINDER TO BE AT FAULT. REPLACED THE MASTER CYLINDER HOSE, AND RESEALED THE MASTER CYLINDER. PERFORMED BLAKE BLEEDING PROCEDURES WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20210525001 · FAA SDRS
O · 2017-07-05 Matched by certificate designator
ATA 5740

WHILE PREFORMING MAINTENANCE, A CRACK WAS DISCOVERED IN THE RT MAIN ACTUATOR ATTACH BRACKET.

Source: SDR HYIA20170705003 · FAA SDRS
O · 2015-07-29 Matched by certificate designator
ATA 3243

LEFT FOOT BRAKE, NO PRESS ON LT SIDE, NO BRAKING ACTION LT SIDE. INSPECTED LT BRAKE LININGS, CHECKED FOR LEAKS, NO DEFECTS NOTED. SERVICED MASTER CYLINDER WITH FLUID. OPERATIONS CHECKED GOOD.

Source: SDR HYIA20150804002 · FAA SDRS
O · 2015-01-23 Matched by certificate designator
ATA 5410

DURING SCHEDULED INSPECTION EVENT, THE RT NACELLE INBD ENG BEAM WAS FOUND TO BE CRACKED AT UPPER FWD INBD RADIUS IN THE AREA CORRESPONDING TO FWD INBD ENG MOUNT. A SUPPLEMENT TO THIS SDR WILL BE SUBMITTED TO ILLUSTRATE DAMAGE POINT. CORRECTIVE ACTION WILL BE COMPLETE DISASSEMBLY OF INBD ENG BEAM FOR INSPECTION & REPLACEMENT OF ALL DAMAGED PARTS.

Source: SDR HYIA01242015001 · FAA SDRS
O · 2013-12-02 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, OEM PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414054 · FAA SDRS
K J · 2012-12-08 Matched by certificate designator
ATA 8550

THE PILOT REPORTED A STEADY LOSS OF RT ENGINE OIL PRESSURE AFTER TAKEOFF. ENGINE SHUTDOWN AND FEATHERED BEFORE OIL PRESSURE REACHED THE RED LINE. DIVERTED BACK TO THE DEPARTURE. DURING MX INSPECTION, A LOOSE B-NUT WAS ALSO FOUND ON THE OIL PRESSURE LINE TO THE WASTE GATE. B-NUT TIGHTENED, AND ACFT RELEASED FOR SERVICE.

Source: SDR HYIA20121210001 · FAA SDRS
O · 2011-06-06 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, OEM PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415062 · FAA SDRS
O · 2010-08-25 Matched by certificate designator
ATA 3211

CREW REPORTED, ON TOUCHDOWN, LT MAIN GEAR BRAKE APPEARED TO LOCK UP. DIRECTIONAL CONTROL PARTIALLY MAINTANED, BUT DID VEER OFF RUN WAY ON TO GRASS APRON. MX INSPECTED LT MAIN GEAR AND FOUND TORQUE LINK CTR PIVOT BOLT AND ASSOCIATED HARDWARE MISSING. R & R LT MAIN GEAR UPPER AND LOWER TORQUE LINK ASSEMBLIES AS A PRECAUTIONARY MEASURE. ACFT RETURNED TO SERVICE.

Source: SDR HYIA67886LFTTQLNK · FAA SDRS
J · 2009-12-30 Matched by certificate designator
ATA 3233

CREW REPORTED WITH GEAR RETRACTED, RT MAIN GEAR DOWNLOCK LIGHT ILLUMINATED. CREW EXTENDED GEAR USING EMERGENCY EXTENSION SYS. LANDED WITHOUT INCIDENT. MX REMOVED AND REPLACED RT MLG ACTUATOR. COMPLIED WITH GEAR SWINGS, CHECK NORMAL, ACFT RELEASED BACK TO SERVICE.

Source: SDR HYIA67886RTMLG · FAA SDRS
O · 2009-05-11 Matched by certificate designator
ATA 2400

CREW REPORTERD AVIONICS MASTER SWITCH FAILED TO TURN OFF. WORKED OK AFTER SEVERAL ATTEMPTS. MAINTENANCE REMOVED AND REPLACED SWITCH AS A PRECAUTIONART MEASURE.

Source: SDR HYIA67886AA · FAA SDRS
O · 2009-03-24 Matched by certificate designator
ATA 3297

PILOT DID NOT HAVE THREE DOWN AND LOCK GREEN LIGHTS. MX INSPECTED AIRCRAFT FOUND BAD C/B AND ONE BAD BULB ON INDICATOR. MX REPLACED C/B AND BULB. PERFORMED REQUIRED INSPECTIONS AND OPERATIONAL CHECKS AND RETURNED ACFT TO SERVICE.

Source: SDR HYIA67886 · FAA SDRS
H · 2006-07-21 Matched by certificate designator
ATA 2410

CREW REPORTED AVIONICS MASTER SWITCH ION. MX CHANGED CIRCUIT BREAKER SWITCH.

Source: SDR 1350527N67786 · FAA SDRS
O · 1997-09-15 Matched by certificate designator
ATA 3231

RIGHT LANDING GEAR DOOR CONTROL ROD BROKE AT ROD END, DOOR WOULD HANG DOWN WITH GEAR UP. INSTALLED NEW CONTROL ROD AND RIGGED. NO FURTHER TROUBLE.

Source: SDR 97ZZZX4331 · FAA SDRS