N687PA

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-07-19 Matched by certificate designator
ATA 3350

DURING INSPECTION, THE EMERGENCY LIGHT CIRCUIT BREAKER NUMBER 9 WAS FOUND BE TRIPPED. MAINTENANCE REPLACED EMERGENCY LIGHT SWITCH ASSEMBLY. OPERATIONAL CHECKS WERE GOOD WITH NO FURTHER DEFECTS NOTED AT THAT TIME. BEFORE THE AIRCRAFT FLEW, MAINTENANCE FOUND THE CIRCUIT BREAKER TO BE TRIPPED AGAIN. MAINTENANCE REPLACED RELAY 75LN. OPERATIONAL CHECKS WERE GOOD WITH NO FURTHER DEFECTS NOTED.

Source: SDR 4VAA20230719006 · FAA SDRS
L · 2023-03-27 Matched by certificate designator
ATA 3350

DURING INSPECTION THE FORWARD PROXIMITY LIGHTING STRIP WAS FOUND TO BE PULLED AWAY FROM THE MOUNT AND THE WIRES WERE PULLED OUT. MAINTENANCE REPLACED THE FORWARD PROXIMITY LIGHT STRIP. OPERATIONAL CHECKS WERE GOOD WITH NO FURTHER DEFECTS NOTED.

Source: SDR 4VAA20230327001 · FAA SDRS
L · 2022-10-20 Matched by certificate designator
ATA 3350

DURING INSPECTION, THE MECHANIC DISCOVERED THE FORWARD CABIN FLOOR PROXIMITY LIGHT 31LN IS INOPERATIVE AND DETACHED FROM THE SIDE OF THE AISLE. MAINTENANCE SOLDERED DETACHED WIRES ON THE FLOOR PROXIMITY LIGHT STRIP. OPERATIONAL CHECKS WERE GOOD WITH NO FURTHER DEFECTS NOTED.

Source: SDR 4VAA20221020002 · FAA SDRS
L · 2022-10-20 Matched by certificate designator
ATA 3350

"DURING INSPECTION, THE MECHANIC FOUND THE FLIGHT ATTENDANT EMERGENCY LIGHT SWITCH 7LN ""ARMED"" PORTION OF SWITCH IS INOPERATIVE, AND BULB IS BURNED OUT. FINAL CORRECTIVE ACTION AND PART INFORMATION WILL BE SUBMITTED AS A SUPPLEMENT TO THIS REPORT.

Source: SDR 4VAA20221020003 · FAA SDRS
J · 2022-07-15 Matched by certificate designator
ATA 2100

DURING FLIGHT, THE CREW RECEIVED A CABIN AUTO PRESSURIZATION FAIL MESSAGE. THE CREW FOLLOWED THE QUICK REFERENCE HANDBOOK AND THE MESSAGE DID NOT CLEAR. THEY DIVERTED THE AIRCRAFT AND LANDED WITHOUT FURTHER INCIDENT. MAINTENANCE REPLACED THE AUTO PRESSURIZATION CONTROLLER. OPERATIONAL CHECKS WERE GOOD WITH NO FURTHER DEFECTS NOTED ***THE FINAL CORRECTIVE ACTION AND PART INFORMATION IS BEING SUBMITTED AS A SUPPLEMENT TOT HE REPORT ORIGINALLY FILED ON 7/18/2022.***

Source: SDR 4VAA20220715001 · FAA SDRS
Y M · 2018-01-05 Unresolved
ATA 7200

RIGHT ENGINE FAILURE, DID NOT ATTEMPT RESTART. ENGINE AUTOSHUT DOWN IN FLIGHT.

Source: SDR PNSA2018010501 · FAA SDRS
M Y J · 2017-07-18 Unresolved
ATA 7200

RT ENGINE INFLIGHT FAILURE. PILOT REPORT STATED THAT FO WAS IN CONTROL AT 31,000 FEET, AS THEY STARTED TO DESCENT, THE FO PULLED POWER BACK AT WHICH TIME THE RIGHT ENGINE GAVE AN OVERTEMP WARNING AND A RT ENGINE MAINTENANCE MESSAGE AND RTENGINE FAULT. THE FO WENT TO GIVE CONTROL TO THE CAPTAIN AND BY THE TIME HE HAD CONTROL, THE RIGHT ENGINE DID AN AUTO SHUT DOWN.

Source: SDR PNSA2017072403 · FAA SDRS
L · 2017-07-05 Unresolved
ATA 3350

EMERGENCY LIGHTING POWER SUPPLY FAILED DURING FUNCTION CHECK

Source: SDR PNSA2017070501 · FAA SDRS
O · 2017-05-02 Unresolved
ATA 3210

GEAR UNSAFE - RT MLG YELLOW DOWN ARROW.

Source: SDR 2017FA0000175 · FAA SDRS