N701QS

BOMBARDIER INC BD-100-1A10 · 2019 · Valid Registration

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
NETJETS AVIATION, INC. (DXTA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

A E J · 2026-05-22 Matched by certificate designator
ATA 7200

ON CLIMBOUT SHORTLY AFTER TAKEOFF, RECEIVED A STRONG VIBRATION FOLLOWED BY A L ENG EXCEEDANCE CAS & A OVERTEMP ON ITT. REDUCED THUST LEVER TO BRING ITT DOWN. RECEIVED A LT ENG VIBRATION CAS FOLLOWED BY A LT ENG FLAMEOUT CASS. VIBRATION DECREASED BUT NEVER WENT AWAY. REMOVED UNSERVICEABLE LT ENGINE, IAW AMM 71-00-01-000-801. INSTALL CUSTOMER PROVIDED REPAIRED ENGINE INSTALLED ON REPLACEMENT LT ENGINE. ALL POST OPS CHECK COMPLETED OPS CHKD GOOD.

Source: SDR DXTA2026052608193 · FAA SDRS
B · 2023-12-19 Matched by certificate designator
ATA 2150

CABIN ODOR IN CABIN. "SOCKS OR WET DOG" SMELL. SEEMS MORE PRONOUNCED AT SEA LEVEL, DENSE AIR. TRANSFERRING TO APU SEEMS TO INCREASE THE SMELL BUT IT MAY JUST BE THE HIGHER FLOW OF AIR. REMOVED AND REPLACED ACM DUE TO TORQUE CHECKS FAIL . OPS/LEAK CHECKS REQUIRED. ACM OPS/LEAK CHECKED GOOD. ALL MX COMPLETED IAW AMM CHAPTER 21-52-13.

Source: SDR DXTA2023122010381 · FAA SDRS
J · 2022-05-26 Matched by certificate designator
ATA 7930

RIGHT AND LEFT ENGINES - ENGINE OIL PRESSURE: DURING CRUISE AT FL370 THE RIGHT ENGINE OIL PRESS LOW CAS MESSAGE ILLUMINATED ALOMG WITH RED LOW OIL PRESSURE.//CORRECTIVE ACTION//FOUND OIL CAP NOT SECURED, SECURED CAP. PERFORMRMED ENGINE RUNS WITH NO FURTHER LEAKS OR DEFECTS NOTED

Source: SDR DXTA2022052662760 · FAA SDRS
E F · 2014-04-02 Matched by certificate designator
ATA 2720

AT FLIGHT LEVEL 210 AND AT 345 KNOTS, THE ACFT HAD A BUZZING SOUND & AIRFRAME VIBRATION FELT IN CONTROLS. SHORTLY AFTER HAD A VIOLENT UNCOMMANDED RUDDER LEFT WITH NO PILOT INPUT. THE ACFT JERKED HARD FOR A FEW SECONDS. PERFORMED A NORMAL LANDING. PERFORMED THOROUGH BORESCOPE INSPECTION OF NR 1 & 2 ENGINES WITH NO SIGNIFICANT FINDINGS. PERFORMED FIVE POINT ENGINE CALIBRATION RUNS OF BOTH ENGINES WITH ALL PARAMETERS TO BE WITHIN LIMITS. PERFORMED OPS CHECK OF RUDDER BIAS SYSTEM WITH NO DEFECTS NOTED. INSTALLED P2.8 MOISTURE TRAP AND P2.8 TRANSDUCER LINE WITH NO DEFECTS NOTED. SWAPPED P3 TRANSDUCERS FOR FURTHER OBSERVATION. ALL WORK PERFORMED IAW EMM 75-30-03, 753009, 72-00-00 & AMM 27-20-35.

Source: SDR DXTA2014040405716 · FAA SDRS
J · 2013-03-29 Matched by certificate designator
ATA 2730

ELEVATOR FEEL FAIL ILLUMINATED TWO TIMES DURING FLIGHT. REMAINING ON FOR 30-60 SECONDS EACH TIME. R & R Q FEEL SERVO ACTUATOR IAW CMP 273014. PERFORMED STALL PROTECTION AND Q FEEL ACTUATOR ADJUSTMENT TEST IAW CMP 273030. NO DEFECTS NOTED.

Source: SDR DXTA201304015344 · FAA SDRS
B · 2012-08-24 Matched by certificate designator
ATA 3030

HEAVY SULFUR ODOR IN COCKPIT WITH APU OPERATING WITH AVIONICS ON. ODOR IS NOT ASSOCIATED WITH ENVIRONMENTAL SYS. NO VISIBILE SMOKE WAS NOTICED. FOUND "PROBE HEAT" SWITCH IN OVERRIDE POSITION. THIS SETTING DELIVERS FULL POWER TO ALL PROBES AND TAKES THE AOA'S FROM LOW TO FULL POWER. OVERHEATING OF THE PROBES WAS CAUSING THE ODOR. INSPECTED PROBES AND FOUND NO DEFECTS. PLACED SWITCH IN AUTO POSITION, ODOR DID NOT RETURN. WORK DONE IAW AMM CH - 30-30-00.

Source: SDR DXTA2012082405105 · FAA SDRS
J · 2011-10-25 Matched by certificate designator
ATA 3610

BLEED PRESSURE AND TEMP HIGH WARNING MESSAGE ILLUMINATED ON TAKEOFF ROLL. PERFORMED ENGINE RUNS FOR OPS CHECK, WITH ECS SYS ON APU, RAN LT ENGINE & RT ENGINE NOTING NO MESSAGES, INSPECTED PRECOOLERS FOR DAMAGE AND BLOCKAGE NOTING NO FAULTS, INSPECTED PRECOOLER BY PASS VALVE INDICATOR WITH NO FAULTS NOTED. INSPECTED PRECOOLER TEMP SENSOR NOTING NO FAULTS, REF MM 21.00-00.

Source: SDR DXTA2011102504762 · FAA SDRS
A B J · 2010-07-16 Matched by certificate designator
ATA 7250

ABOUT 45 MINUTES INTO THE FLIGHT, CLIMBING THRU FL 360, CREW HEARD A LOUD "BANG", FELT A VIBRATION, ITT BEGAN AN IMMEDIATE CLIMB, FOLLOWED BY THE "FIRE" LIGHT AND SMOKE IN THE CABIN. CREW BROUGHT THE THROTTLE TO IDLE, SHUT THE ENGINE DOWN VIA THE FUEL CUTOFF SWITCH, DECLARED AN EMERGENCY AND WAS VECTORED BY ATC TO THE NEAREST SUITABLE AIRPORT.

Source: SDR DXTA2010071604156 · FAA SDRS
B J · 2010-07-16 Matched by certificate designator
ATA 7200

RT ENGINE SHUTDOWN INFLIGHT DUE TO VIBRATION DETECTOR AT MAX LEVEL WITH CORRESPONDING RISING HIGH ITT LEVEL (NOT IN RED) AND ENGINE FIRE CAS MESSAGE. THERE WAS ALSO THE SMELL OF SMOKE IN THE CABIN BUT NOT VISIBLE. ENGINE WAS SECURED BY POWER TO IDLE AND FUEL CUTOFF SWITCH. THE ENGINE DID NOT AUTO SHUTDOWN. R & R RT ENGINE WITH RENTAL UNIT. PERFORMED OPS CHECKS AND LEAK CHECKS WITH NO DEFECTS NOTED, REF MM 71-00-00.

Source: SDR DXTA201007160415 · FAA SDRS
M J · 2010-03-15 Matched by certificate designator
ATA 2432

EMERGENCY BATTERY OVERHEATED IN FLIGHT; TEMP WENT TO 170 DEGREES F, VOLTS REMAINED AT 26.7. R & R EMERGENCY BATTERY WITH O/H UNIT MM 24-30-20, CMP 243019. OPS CHECKS GOOD.

Source: SDR DXTA2010031604036 · FAA SDRS
O · 2008-07-14 Matched by certificate designator
ATA 3414

NO AIRSPEED ON TAKEOFF ROLL, ABORTED T/O. VISUALLY INSPECTED PITOT TUBES AND LINES. PERFORMED RECONNECT CHECK ON PILOT COPILOT & STANDBY PITOT/STATIC SYSTEM'S REF MM 34-11-00 PGS 602-606 SYSTEM OPS CHECK GOOD AND LEAK CHECK GOOD.

Source: SDR DXTA200803172 · FAA SDRS
O · 2007-11-17 Matched by certificate designator
ATA 5730

DURING LANDING AND AFTER TOUCHDOWN, THE AIRCRAFT DEPARTED THE LT SIDE OF THE RUNWAY. DAMAGE NOTED ON THE LOWER IB SECTION OF THE RT WING, DAMAGE NOTED ON THE RT WING IB LEADING EDGE, AND DAMAGE NOTED ON THE RT KRUEGER FLAP.

Source: SDR DXTA200702614 · FAA SDRS
B · 2007-04-24 Matched by certificate designator
ATA 2120

ACRID ELECTRICAL BURNING SMELL EMINATING FROM BEHIND LT PILOT SEAT IN COCKPIT. CHECKED ALL CB'S, NOTHING FOUND (POPPED). [4-27-07] PERFORMED ENG RUN AND APCS RUNS FOR COCKPIT SMELLS, RUNS SATISFACTORY. ACCESSED L/R RELAY PANEL FOUND SATISFACTORY. ACCESSED FWD EQUIPMENT CLOSET CB CHR105& CHR203 POPPED. RESEAT OPS CK 115AC OUTLET GOOD. .RE-RACK AIRSHOW COMPUTER. OPS CK GOOD. ACCESSED L/H PILOT WINDSHIELD HEAT T/B. AT OVERHEAD FOUND SATISFACTORY. OPS CHECK DOOR MOTOR GOOD. COULD NOT DUPLICATE BURNING ODOR FOUND AIRCRAFT SATISFACTORY FOR FLIGHT WORK DONE IAW G2000 M/M CH 5-00-00 AND CH 24-00-00.

Source: SDR DXTA200702137 · FAA SDRS
N · 2006-11-18 Matched by certificate designator
ATA 2612

WE WERE LEVEL AT FLIGHT LEVEL 350 WHEN THE (APU FIRE LIGHT) AND BELL CAME ON. WE FIRED THE BOTTLE AND THE FIRE LIGHT STAYED ON. REMOVED AND REPLACED RT FIRE BOTTLE IAW MM 26-20-05. FIRE LOOP FOUND BAD AND REPLACED. APU FIRE DETECTION SYSTEM WAS OPS CHECKED AND CHECKED GOOD.

Source: SDR DXTA200601734 · FAA SDRS