N702FL

CESSNA 750 · 1999 · Valid Registration

Registered owner: CARLISLE01 LLC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
WHEELS UP PARTNERS LLC (VQMA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1981-10-29 Unresolved
Piper PA-28 None injuryoperator not yet resolved
Source: NTSB case ATL82FKG04
Accident · 1978-11-16 Unresolved
Piper PA-28 None injuryoperator not yet resolved
Source: NTSB case MIA79DLD17

Maintenance disclosures

B · 2021-08-09 Matched by certificate designator
ATA 2150

FLIGHT CREW EXPERIENCED A STRONG FIRE/SMOKE SMELL DESCENDING THROUGH FL180. FLIGHT CREW SHUT LEFT PACK OFF PER CHECKLIST, SMELL WENT AWAY. TROUBLESHOOTING FOUND THE LEFT HAND AIR CYCLE MACHINE SEIZED. A SERVICEABLE UNIT WAS INSTALLED WITH NOT FURTHER ANOMALIES NOTED.

Source: SDR VQMA2021071800003 · FAA SDRS
B · 2015-10-21 Matched by certificate designator
ATA 2120

AIRCRAFT LANDED & TAXIED TO THE FBO NORMALLY, AFTER ENG SHUTDOWN, WITH APU RUNNING, THE CABIN BEGAN TO FILL WITH SMOKE & CREW NOTED WARMER THAN USUAL AIR COMING FROM AIR VENTS. DURING THE FLIGHT, PAXS REPORTED & SMOKE ODOR BRIEFLY BUT NOT SMOKE OR OTHER WARNINGS WERE NOTED. THE ODOR DISSIPATED QUICKLY. ALL OCCUPANTS EXITED THE PLANE SAFELY THROUGH THE MAIN ENTRY DOOR AS THE CREW SHUTDOWN THE ACFT. NO DAMAGE TO THE ACFT WAS NOTED. FOUND THE FWD ACM FAILED. IT WAS REPLACED & OPERATIONAL CHECKS WERE FOUND SATISFACTORY.

Source: SDR DJFA20151021001 · FAA SDRS
O · 2010-12-31 Matched by certificate designator
ATA 5610

DURING FLIGHT, CREW NOTED THE COPILOTS WINDSHIELD HEAT FAIL MESSAGE ON THE EICAS. SHORTLY AFTER THE NOTIFICATION, THE COPILOTS WINDSHIELD SHATTERED. THE ACFT DIVERTED AND LANDED SAFELY. MX CONFIRMED THE FAILED WINDSHIELD AND REPLACED IT.

Source: SDR DJFA2011003 · FAA SDRS
K · 2010-05-31 Matched by certificate designator
ATA 2910

AFTER LANDING, CREW REPORTED A LARGE PUDDLE OF HYD FLUID UNDER THE ACFT. MX FOUND THE NR 3 BRAKE LINE RUPTURED. THE LINE WAS REPLACED.

Source: SDR DJFA2010014 · FAA SDRS
K J · 2010-02-13 Matched by certificate designator
ATA 2910

IN FLIGHT, CREW REPORTED LOSS OF HYD FLUID. ACFT DIVERTED AND LANDED SAFELY. MX FOUND FLUID LEAKING FROM A FAILED O-RING ON THE HYD SYS 'A' PRESSURE SWITCH. THE O-RING AND PRESSURE SWITCH WERE REPLACED.

Source: SDR DJFA201003 · FAA SDRS
O · 2009-06-01 Matched by certificate designator
ATA 5510

DURING A SCHEDULED MX INSP, TECHS FOUND A CRACK IN THE RT INBD HORIZONTAL STABILIZER HINGE BRACKET. REQUIRED NDT INSP WAS PERFORMED AND THE CRACK WAS FOUND TO BE LESS THAN 0.49", THEREFORE A 50 HOUR RECURRING INSP HAS BEEN SCHEDULED FOR THIS ACFT.

Source: SDR DJFA2009029 · FAA SDRS