N705FX

CESSNA 208B · 1995 · Valid Registration

Registered owner: FEDERAL EXPRESS CORPORATION, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EMPIRE AIRLINES, INC. (COEA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-05-13 Matched by certificate designator
ATA 2497

FLT. 8676 ENROUTE ANC-HOM AIR TURNBACK DURING CLIMBOUT, THE PILOT RECEIVED A STANDBY POWER ELECTRIC INOP ALERT. THE AIRCRAFT WAS RETURNED TO ANC. NO EMERGENCY WAS DECLARED. LANDED WITHOUT FURTHER INCIDENT. CORRECTIVE ACTION: THE ISSUE WAS DEFERRED AND THE AIRCRAFT WAS RETURNED TO SERVICE. THE DEFERRAL WAS CLEARED FOLLOWING AN OPS CHECK OF THE STANDBY POWER. NO DEFECTS NOTED.

Source: SDR COEA2025051402705 · FAA SDRS
K · 2017-01-25 Matched by certificate designator
ATA 2910

AFTER ARRIVA, THE PILOT NOTED DURING TAXI THAT THE RIGHT BRAKE WAS INOPERATIVE. MAINTENANCE TROUBLESHOT AND FOUND BRAKE FLUID LEAK AND DURING THE OPS CHECK OF THE BRAKES, FOUND A CRACK IN THE RT PARKING BRAKE LINE. REPLACED THE RT PARKING BRAKE LINE. LEAK CHECKS AND TAXI CHECKS GOOD. AIRCRAFT RETURNED TO SERVICE.

Source: SDR COEA2017012501705 · FAA SDRS
K B · 2015-09-16 Matched by certificate designator
ATA 7331

FLIGHT 7805 AIR TURN BACK. AFTER TAKEOFF, THE PILOT REPORTED A FUEL SMELL IN THE COCKPIT. THE PILOT ELECTED TO RETURN WHERE THE ACFT WAS GNDED. NO EMER WAS DECLARED. TROUBLE SHOT & FOUND TWO LOOSE B NUTS ON THE FUEL FLOW TRANSMITTER. TIGHTENED B NUTS TO SPEC, TEST RAN & LEAK CHECKED. ACFT RETURNED TO SERVICE.

Source: SDR COEA2015091601705 · FAA SDRS
B J · 2004-10-23 Matched by certificate designator
ATA 2420

ENROUTE, PILOT REPORTED THE STANDBY ELECTRIC POWER (ON) AND (INOP) ANNUNCIATOR LIGHTS ILLUMINATED. STANDBY POWER SYSTEM WAS INOPERATIVE. PILOT REPORTED SMELLING SMOKE. NO EMERGENCY WAS DECLARED, HOWEVER, THE EMERGENCY EQUIPMENT RESPONDED. AIRCRAFT LANDED WITHOUT INCIDENT. MAINTENANCE REPLACED THE STANDBY POWER RELAY AND ALTERNATOR CONTROL UNIT. REPAIRED SHORTED GENERATOR CONTACTOR SENSE WIRE AT GCU. AIRCRAFT WAS RETURNED TO SERVICE. NO CIRCUIT BREAKERS POPPED.

Source: SDR COE2004F00002 · FAA SDRS