N708FL

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLIGHT OPTIONS LLC (DJFA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

R · 2015-11-26 Matched by certificate designator
ATA 7200

DURING CLIMB OUT, CREW REPORTED THE LT ENG SURGED & ROLLED BACK MULTIPLE TIMES. ACFT RETURNED TO THE DEPARTURE AIRPORT & LANDED SAFELY. REPLACED THE NR 2 ENG.

Source: SDR DJFA20151126001 · FAA SDRS
R J · 2015-11-20 Matched by certificate designator
ATA 7697

CREW REPORTED ENG POWER ROLL BACK INTERMITTENTLY. ACFT LANDED SAFELY. REPLACED THE ENG CONTROL B WIRE HARNESS.

Source: SDR DJFA20151120002 · FAA SDRS
R J · 2015-11-14 Matched by certificate designator
ATA 7321

DURING CLIMB, LT ENG POWER FLUCTUATED & ROLLED BACK 10 PERCENT 3 TIMES. AFTER THE THIRD ROLL BACK, FAN DAMAGE CAS MSG ILLUMINATED. ACFT LANDED SAFELY & NO ENG DAMAGE WAS NOTED. REPLACED THE LT ENGINE B SYS FADEC. SYS OPERATIONAL CHECKS WERE FOUND SATISFACTORY.

Source: SDR DJFA20151114001 · FAA SDRS
R · 2015-11-06 Matched by certificate designator
ATA 7530

DURING CLIMB, LT ENG POWER FLUCTUATED & ROLLED BACK UP TO 10 PERCENT, THEN RECOVERED. FLUCTUATIONS CEASED UPON LEVEL OFF AT CRUISING ALTITUDE. ON LANDING NOTED MULTIPLE ERROR CODES IN THE SYS. TROUBLE SHOT THE SYS & FOUND THE CVG VLV DEFECTIVE. THE UNIT WAS REPLACED.

Source: SDR DJFA20151106001 · FAA SDRS
E J · 2015-09-22 Matched by certificate designator
ATA 7200

ON CLIMB OUT, CREW FELT VIBRATION IN THE LT ENG & 20 SECONDS LATER RECEIVED A LT FAN DAMAGE CAS MSG. PERFORMED THEIR CHECKLIST, DECLARED AN EMER & DIVERTED BACK SAFETY. AT THE MOMENT, WE SUSPECT A BIRD, FOD, WAS INGESTED INTO THE ENG. FOUND NO DAMAGE TO THE ENG. ENG RUNS WERE PERFORMED WITH NO ABNORMAL RESULTS & THE ACFT WAS RELEASED FOR SERVICE.

Source: SDR DJFA20150922001 · FAA SDRS
K J · 2012-04-12 Matched by certificate designator
ATA 2910

ON DESCENT, CREW REPORTED GEAR TOOK EXCESSIVE TIME TO EXTEND AND NOTED FLUCTUATIONS IN THE A-SYS HYD QTY INDICATION. EMERGENCY WAS DECLARED BUT THE ACFT LANDED SAFELY. MX FOUND THE RT MLG ACTUATOR FLEX LINE LEAKING. THE LINE WAS REPLACED AND ALL LEAK AND OPS CHECKS WERE SATISFACTORY.

Source: SDR DJFA20120412001 · FAA SDRS