N70AX

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2010-02-16 Matched by certificate designator
ATA 3260

WHEN SELECTING "GEAR DOWN" ON APPROACH TO DESTINATION AIRPORT THERE WAS NO RT DOWNLOCK "GREEN" ANNUNCIATOR. LANDING GEAR WAS CYCLED 5 TIMES. THE 5TH TIME SHOWED "3 GREEN" AND ACFT WAS LANDED WITHOUT INCIDENT. ACFT WAS JACKED AND GEAR WAS SWUNG. FOUND INTERMITTENT RT MAIN GEAR DOWN LOCK SWITCH. WIRING WAS BROKEN INTERNALLY RT AT THE SWITCH POTTING. REPLACED SWITCH WITH NEW PART. OPS CHECK SATISFACTORY AND ACFT RELEASED FOR SERVICE.

Source: SDR 2010F00045 · FAA SDRS
O · 2009-09-30 Matched by certificate designator
ATA 5410

AFTER TAKEOFF, THE FLIGHT CREW NOTICED AIRFRAME VIBRATION. ACFT LANDED AT THE CLOSEST AIRPORT WITHOUT INCIDENT. A VISUAL INSPECTION OF THE RT COWLING SHOWED THAT THE FWD OTBD 2 LATCHES WERE UNLATCHED AND THE AFT OTBD LATCH WAS SECURED. THE UPPER AND LOWER COWLING SUSTAINED MINOR DAMAGE. CAUSE WAS A FAILURE TO SECURE THE TWO FWD LATCHES AFTER CHECKING ENGINE OIL. PROCEDURES FOR ENSUING A THOROUGH PREFLIGHT INSPECTION SHOULD BE REINFORCED AND ALL PERSONNEL SHOULD FOLLOW A COMPLETE PREFLIGHT INSPECTION AFTER THE ACFT HAS BEEN DISTURBED FOR ANY REASON PRIOR TO FLIGHT. (K)

Source: SDR RMV2009F00001 · FAA SDRS