N712AS

EA VISION EA J100 · Valid Registration

Registered owner: AGRI SPRAY DRONES LLC, MO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2008-08-02 Matched by certificate designator
ATA 3442

FLIGHT WW171. DEPARTED MIV TO IAD. CLIMBING OUT OF 8000 FT, CREW NOTICED THE RADAR SCREEN START TO FLICKER. IMMEDIATELY SHUT THE RADAR OFF. CREW DETECTED WHAT APPEARED TO BE SMOKE RELATED TO ELECTRICAL FIRE. CREW SAW HEAVY SMOKE COMING OUT OF THE DASHBOARD. DECLARED AN EMERGENCY. AFTER PERFORMING CORRECT CHECKLIST & ASSESSING THE SITUATION SMOKE HAD DISSIPATED & CAPT DECIDED THAT THERE WAS NO LONGER AN EMERGENCY. REQUESTED TO FLY BACK TO MIV. LANDED AT 1405 WITH NO ADDITIONAL PROBLEMS. INSPECTED THE COCKPIT & DETERMINED THE WEATHER RADAR CONTROL UNIT (CRT) HAD SHORTED OUT INTERNALLY. INSPECTED BEHIND THE INSTRUMENT PANEL & ASSOCIATED WIRING GOING TO THE WEATHER RADAR CONTROL UNIT (CRT), & NO DEFECTS NOTED. REMOVED THE BAD CRT & INSTALLED & INSPECTED CRT. PERFORMED OPERATIONAL CHECKS OF THE SYSTEM. ALL OPERATIONAL CHECKS GOOD WITH NO DEFECT NOTED. (S)

Source: SDR WWQ2008F00000 · FAA SDRS
P · 2008-08-02 Matched by certificate designator
ATA 3442

AC WAS DISPATCHED, THE CREW CAPTAIN AND F/O DEPARTED AT 13:40 ENROUTE. AT APPROX 13:50, WHILE CLIMBING OUT OF 8000 FEET, PILOTS NOTICED THE RADAR SCREEN START TO FLICKER. CAPT IMMEDIATELY SHUT THE RADAR OFF. A SHORT WHILE LATER PILOTS SMELLED WHAT APPEARED TO BE SMOKE RELATED TO ELECTRICAL FIRE. PILOTS THEN SAW HEAVY SMOKE COMING OUT OF THE DASHBOARD. CAPT THEN DECLARED AN EMERGENCY, INITIALLY REQUESTED TO DIVERT, DUE TO THE AVAILABILITY OF LONGER RUNWAYS AND MUCH BETTER EMERGENCY EQUIPMENT IN CASE IT WAS NEEDED. AFTER PERFORMING CORRECT CHECKLIST AND ASSESSING THE SITUATION THE SMOKE HAD DISSIPATED AND CAPT DECIDED THAT THERE WAS NO LONGER AN EMERGENCY. AT THAT POINT REQUESTED TO FLY BACK TO DEPARTURE AND LANDED AT 14:05 WITH NO ADDITIONAL PROBLEMS. INSPECTED COCKPIT AND DETERMINED THE WEATHER RADAR CONTROL UNIT (CRT) HAD SHORTED OUT INTERNALLY. INSPECTED BEHIND THE INSTRUMENT PANEL AND ASSOCIATED WIRING GOING TO THE WEATHER RADAR CONTROL UNIT(CRT) AND NO DEFECTS NOTED. REMOVED THE BAD CRT AND INSTALLED INSPECTED CRT, PERFORMED OPS CHECKS OF THE SYS . ALL OPERATIONAL CHECK GOOD WITH NO DEFECT NOTED. (K)

Source: SDR WWQ2008F00003 · FAA SDRS