N717XJ

CESSNA 750 · 2003 · Valid Registration

Registered owner: MACH .92 LEASING LLC, NC (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
XOJET Aviation LLC (AWKA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2024-05-24 Matched by certificate designator
ATA 3260

(DIVERTED) (DECLARED EMER.) CREW REPORTED DURING CLIMB AS GEAR MADE THE UPLOCKS MULTIPLE CAS MESSAGES POSTED, PITCH TRIM, YAW DAMP, MACH TRIM. MESSAGES BEGAN TO EXTINGUISH, STAB. TRIM REMAINED INOP. PERFORMING AFCS FAULTS PER TECH SUPPORT. OPS CHECKS GOOD ON GROUND AT THIS TIME. NO DEFECTS NOTED. PERFORMED GEAR SWINGS AND COULD NOT DUPLICATE DISCREPANCY. IAW HONEYWELL SYSTEM TEST AND FAULT ISOLATION MANUAL.

Source: SDR AWKA202405270171 · FAA SDRS
J · 2024-05-24 Matched by certificate designator
ATA 2700

(DECLARED EMER.) (DIVERTED) CREW REPORTED DURING CLIMB AS GEAR MADE THE UPLOCKS MULTIPLE CAS MESSAGES POSTED, PITCH TRIM, YAW DAMP, MACH TRIM. MESSAGES BEGAN TO EXTINGUISH, STAB. TRIM REMAINED INOP. PERFORMED AFCS FAULTS PER TECH SUPPORT, OPS CHECKS GOOD ON GROUND AT THIS TIME, NO DEFECTS NOTED. PERFORMED GEAR SWINGS AND COULD NOT DUPLICATE DISCREPANCY. IAW SYSTEM TEST AND FAULT ISOLATION MANUAL.

Source: SDR AWKA202405290003 · FAA SDRS
J · 2019-10-18 Matched by certificate designator
ATA 2740

WHILE DESCENDING, THE FLIGHT CREW RECEIVED AN AMBER PITCH FEEL FAIL CAS MESSAGE. THE MESSAGE WAS INTERMITTENT AT FIRST, BUT THEN STAYED ON UNTIL LANDING. THE FLIGHT CREW FOLLOWED THE CHECK LIST PROCEDURE AN DECLARED AN EMERGENCY FOR A PRIORITY LANDING. THE AIRCRAFT LANDED UNEVENTFULLY. MAINTENANCE CREWS INSPECTED THE AIRCRAFT. AS A PRECAUTION, THE LEFT AND RIGHT ELEVATOR PITCH FEEL LINEAR ACTUATORS WERE REPLACED. OPERATIONAL CHECKS PERFORMED SATISFACTORILY AND THE AIRCRAFT RELEASED BACK INTO SERVICE.

Source: SDR AWKA 2019102101 · FAA SDRS
J · 2016-10-02 Matched by certificate designator
ATA 3230

DURING LANDING GEAR EXTENSION, FLIGHT CREW NOTED 3 GREEN GEAR POSITION INDICATIONS ALONG WITH A RED UNLOCK LIGHT ILLUMINATED. WHILE IN A HOLDING PATTERN, THE RED UNLOCK LIGHT EVENTUALLY EXTINGUISHED. FLIGHT CREW ACCOMPLISHED THE EMERGENCY GEAR BLOW DOWN PROCEDURE PER THE CHECKLIST, AND AS A PRECAUTION, DECLARED AN EMERGENCY. AFTER A CONTROL TOWER FLYBY TO CONFIRM THAT 3 GEAR WERE INDEED DOWN, THE CREW LANDED UNEVENTFULLY. THE AIRCRAFT WAS FERRIED TO SMF FOR MX. CURRENTLY, THERE IS NO EXACT FAULT FOUND, BUT A RH MLG DOWNLOCK SWITCH IS A SUSPECT FAILED PART. A SUPPLEMENTAL SDR WILL BE SUBMITTED WHEN MAINTENANCE IS COMPLETE WITH ALL OF THE FINDINGS. DURING TROUBLESHOOTING OF THE LANDING GEAR INDICATION SQUAWK, A FAULTY RH MLG DOWNLOCK SWITCH (P/N 6-0407-1) WAS FOUND. THE SWITCH WAS REPLACED WITH A NEW ASSEMBLY. SATISFACTORY GEAR SWING OPERATIONAL CHECKS WERE PERFORMED, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR AWKA201610100002 · FAA SDRS