N721AF

PILATUS AIRCRAFT LTD PC-12/47E · 2017 · Valid Registration

Registered owner: AVIATION17 LLC, NH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
COBALT AIR, LLC (6CBA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2019-09-05 Matched by certificate designator
ATA 2120

PROBLEM: THE FLIGHT CREW REPORTED " BURNING SMELL COMING FROM ACS SYSTEM". RESOLUTION: MAINTENANCE WAS DISPATCHED TO THE AIRCRAFT, THE FOLLOWING ACTION WAS ACCOMPLISHED " VISUALLY INSPECTED ACS DUCTING AND CLAMPS AND ENGINE COMPARTMENT. NO DEFECTS NOTED. RAN AIRCRAFT AND HEAT FOR 10 MIN IAW AMM 12-B-71-00-00-00A-903S-A. OPS CHECK GOOD. NO SMELLS. THE AIRCRAFT WAS RELEASED.

Source: SDR 6CBA2019090519187 · FAA SDRS
J · 2014-07-28 Matched by certificate designator
ATA 3211

AFTER DEPARTURE RT GEAR UNSAFE LIGHT ILLUMINATED ON GEAR RETRACTION. THE ACFT DIVERTED & LANDED SAFELY. INSPECTION OF THE RT LG REVEALED THE LOWER RT LG ACTUATOR BOLT BROKEN AT THE NUT ATTACHMENT & WAS WORKING OUT OF THE GEAR MOUNTING HOLE. THE INNER BORE OF THE MLG WAS ALSO FOUND DAMAGED FROM THE BOLT BACKING OUT. THE BOLT PN 532.10.12.218 & MLG FITTING PN 532.10.12.206 WERE REPLACED WITH NEW.

Source: SDR 6CBA20140728131 · FAA SDRS
F · 2012-08-13 Matched by certificate designator
ATA 2740

DURING A TRAINING FLIGHT, THE CREW REPORTED A PITCH TRIM RUNAWAY WITH AUDIBLE WARBLE. STABILIZER TRIM AND AUTO PILOT SYSTEMS WERE OPERATED AND TESTED IAW THE AMM 12-A-27-40-00-00A-903A-A, 12-A-22-10-00-00A-903A-A. PROBLEM COULD NOT BE DUPLICATED. RELAYS K021,K022 AND K241 PN 974.20.01.212 AND 974.20.01.214 WERE CHANGED AS A PRECAUTION. NOTE: RELAYS TIME IN SERVICE ARE AS FOLLOWS K021=1774.3 K022= 4962.8 K241= 4962.8.

Source: SDR 6CBA20120813119 · FAA SDRS
O · 2011-04-03 Matched by certificate designator
ATA 5510

THE HORIZONTAL STABILIZER ATTACHMENT FITTING, WHERE THE PITCH TRIM ACTUATOR IS SECURED TO THE STABILIZER. EACH SIDE OF THE ATTACHMENT FITTING HAS 2 LUGS. ON THE LT SIDE, THESE 2 LUGS ARE SEPARATING. THE GAP WAS MEASURED WITH A FEELER GUAGE, AND FOUND TO BE .406MM. THERE IS NO EVIDENCE OF DAMAGE TO THE STABILIZER. THE BRACKET PN IS 555.10.12.150, ANGLE FITTING LT. THE ACFT MFG ISSUED A REAIR MEMO WITH STATEMENT OF APPROVED DESIGN DATA WITH THE FOLLOWING INSTRUCTIONS. CHECK THE LUGGED FACE OF THE PN 555.1.12.150 (ANGLE FITTING) FOR STRAIGHTNESS. IF WITHIN LIMITS, COMPLETE A VISUAL AND NDT INSP (DYE PENETRANT OR EDDY CURRENT) OF THE ANGLE FITTING AND THE BOLTS. IF NO CRACKS OR DEFECTS NOTED, REINSTALL THE FITTING, USING SEALANT.

Source: SDR 5APR577Y57 · FAA SDRS
O · 2010-01-19 Unresolved
ATA 3240

DURING A LINE CHECK DISCOVERED THE RT BRAKE OTBD BRAKE DISC WAS BROKEN INTO 2 PIECES. REMOVED AND REPLACED BRAKE ASSY IAW MM INSTRUCTIONS.

Source: SDR 5APR577Y26 · FAA SDRS