N727CS

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2003-06-19 Matched by certificate designator
ATA 3241

FLIGHT CREW REPORTED DISPROPORTIONED BRAKE (EFFECTIVENESS) ON LANDING, AT LOW SPEED. REMOVED AND REPLACED ANTI-SKID PRESSURE CONTROL VALVE WITH SERVICEABLE VALVE. TEST TAXI WAS PERFORMED BY SAME FLIGHT CREW AND BRAKES OPERATION WAS NORMAL.

Source: SDR CJP2003F00003 · FAA SDRS
E · 2001-04-17 Matched by certificate designator
ATA 2435

FLIGHT CREW EXPERIENCED AN AIRFRAME RUMBLE DURING TAKEOFF AND OPTED TO RETURN TO LANDING. MAINTENANCE CONFIRMED THE RUMBLE DURING GROUND RUN AND DETRMINED THE LEFT HAND STARTER GENERATOR CAUSING THE RUMBLE. A SERVICEABLE STARTER GENERATOR WAS INSTALLED, RUNUP GOOD AND AIRCRAFT APPROVE FOR RETURN TO SERVICE.

Source: SDR 20010514CW005 · FAA SDRS
B · 2001-01-09 Matched by certificate designator
ATA 3457

PRIOR TO START, PILOT NOTED SMOKE AND BURNT ODOR IN AREA OF THROTTLE QUADRANT WITH SHIPS BATTERIES ON.MAINTENANCE DID TROUBLESHOOT AND DISCOVERED ODOR TO BE FROM GPS CONTROL UNIT IN PEDESTAL (GPS WAS INOPERATIVE) GPS UNIT WAS REMOVED FOR REPAIR AND AIRCRAFT DEFERRED FOR REMOVED GPS. AC RETURNED TO SERVICE.

Source: SDR 20010213CW011 · FAA SDRS