N729PC

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2014-06-30 Matched by certificate designator
ATA 7712

PILOT REPORTED FAULTY TORQUE INDICATION ON RT ENG.

Source: SDR TXHA20140630001 · FAA SDRS
X J · 2011-08-18 Matched by certificate designator
ATA 7314

ON TAKEOFF ROLL THE LT ENGINE FLAMED OUT, PILOT ABORTED TAKEOFF NO FURTHER INCIDENT, RETURNED TO BLOCK. INVESTIGATION BY MX FOUND THE LT FUEL PUMP SHAFT SHEARED.

Source: SDR TXHA20110818001 · FAA SDRS
N · 2011-06-14 Matched by certificate designator
ATA 7722

LT ENGINE ITT SPIKED TO 1150, THEY REDUCED POWER TO FLIGHT IDLE AND ITT REMAINED AT 830 DEG CENT. SHUTDOWN ENGINE AND CONTINUED TO DESTINATION, LANDED WITHOUT INCIDENT. INVESTIGATION, SPLIT ENG AND DID A HOT SECTION INSPECTION AND FOUND NO DEFECTS. TESTED THE T-5 PROBES AND FOUND 7 EA BAD. REPLACED ALL 10 PROBES AS PRECAUTION AND REPLACED THE FUEL NOZZLES AS A PRECAUTION. OPS CHECKS OK ON ENGINE RUN.

Source: SDR 2011F00148 · FAA SDRS
N · 2011-06-14 Matched by certificate designator
ATA 7722

LT ENGINE ITT SPIKED TO 1150 THEY REDUCED POWER TO FLIGHT IDLE AND ITT REMAINED AT 830 DEG CENT. SHUTDOWN ENGINE AND CONTINUED TO DESTINATION, LANDED WITHOUT INCIDENT. INVESTIGATION, SPLIT ENG AND DID A HOT SECTION INSPECTION AND FOUND NO DEFECTS. TESTED THE T-5 PROBES AND FOUND 7 EA BAD. REPLACED ALL 10 PROBES AS PRECAUTION AND REPLACED THE FUEL NOZZLES AS A PRECAUTION. OPS CHECKS OK ON ENGINE RUN.

Source: SDR 2011F00149 · FAA SDRS
J · 1997-10-03 Unresolved
ATA 3297

CLT - FLT 5098 - RIGHT MAIN LANDING GEAR, NO INDICATION OF DOWN AND LOCK. IN FLIGHT EMERGENCY WAS DECLARED. NORMAL PROCEDURES FOLLOWED. AIRCRAFT LANDED WITH NO INCIDENT. MAINTENANCE INSPECTED LANDING GEAR SYSTEM, AND PINNED GEAR. DISCREPANCY DEFERRED TO MSL 092197-2C. AIRCRAFT RELEASED FOR FLIGHT, AIRCRAFT RESTRICTED TO MSL PAGE 32-1/R13/07-15-96, PARA 32, INDEX 3. REPAIRED BROKEN WIRE IN RT STUB WING. RETRACTION CHECKED 10 TIMES. GROUND OPS CHECKED GOOD. AIRCRAFT RELEASED FOR FLIGHT. FLIGHT RESTRICTION REMOVED. (M)

Source: SDR SABA970034 · FAA SDRS
P · 1997-09-21 Unresolved
ATA 3260

CLT - 5098 - RIGHT MAIN LANDING GEAR, NO INDICATION OF DOWN AND LOCK. IN FLIGHT, EMERGENCY WAS DECLARED. NORMAL PROCEDURES FOLLOWED. AIRCRAFT LANDED WITH NO INCIDENT. MAINTENANCE INSPECTED LANDING GEAR SYSTEM, AND PINNED GEAR. DISCREPANCY DEFERRED TO MSP 092197-2C. AIRCRAFT RELEASED FOR FLIGHT, AIRCRAFT RESTRICTED TO MSL PAGE 32-1/R13/07-15-96, PARA 32, INDEX. FOLLOW UP REPORT WILL FOLLOW AT LATER DATE. (M)

Source: SDR SABA970033 · FAA SDRS
J · 1997-08-06 Unresolved
ATA 7261

CLT - FLT 5093 - AFTER DEPARTING CLT, THE NR 1 ENGINE OIL PRESSURE GAUGE STARTED FLUCTUATING. AIRCRAFT RETURNED BACK TO CLT, FOR AN UNEVENTFUL LANDING. MAINTENANCE WAS DISPATCHED TO THE AIRCRAFT. NR 1 ENGINE WAS TROUBLE SHOT AND FOUND ENGINE OIL LEVEL LOW. SERVICED ENGINE WITH OIL. GROUND RUN AND OPS CHECKED GOOD. AIRCRAFT RETURNED TO SERVICE. (M)

Source: SDR SABA9700025 · FAA SDRS
N · 1996-03-22 Unresolved
ATA 7330

CLT/PGV - FLT 5248 - FLIGHT WAS APPROXIMATELY 46 MILES OUT OF CLT WHEN THE LEFT FUEL FILTER CAUTION LIGHT ILLUMINATED DIMLY. THE CAPTAIN CALLED MAINTENANCE CONTROL WITH THE PROBLEM AND HE WAS TOLD TO RETURN TO CLT. UPON THE AIRCRAFT'S RETURN TO CLT, MAINTENANCE PERSONNEL WERE DISPATCHED TO TROUBLESHOOT PROBLEM. LEFT ENGINE FUEL FILTER ELEMENT WAS REMOVED AND INSPECTED FOR CONTAMINATION AND THE FILTER ELEMENT WAS THEN REPLACED AS A PRECAUTIONARY MEASURE. THIS DID NOT FIX THE INDICATION PROBLEM AND THE INDICATION SYSTEM WAS THEN DEFERRED TO THE MSL PER MEL 28-3 UNDER CONTROL NR 0322-10C. THE AIRCRAFT WAS THEN RETURNED TO SERVICE. (X)

Source: SDR SABA9600012 · FAA SDRS