N734CK

BOEING 737-436 · 1993 · Valid Registration

Registered owner: KALITTA CHARTERS II LLC, MI (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2025-10-09 Matched by certificate designator
ATA 5347

MAIN DECK SEAT TRACK AT STA 887 - 986.5 RBL 43.5 CORRODED

Source: SDR K11A2025102200356 · FAA SDRS
O · 2025-09-05 Matched by certificate designator
ATA 5330

REPLACED FUSELAGE SKIN AT STA 907 - 1016, S14R - 20R.

Source: SDR K11A2025121500363 · FAA SDRS
O · 2025-01-12 Matched by certificate designator
ATA 5340

EVIDENCE OF CORROSION ON FRAME ATTACH ANGLE AT STA 500 BETWEEN STRINGER 27R AND 26R.

Source: SDR K11A2025040200310 · FAA SDRS
N · 2024-08-13 Matched by certificate designator
ATA 2700

DURING CLIMB SOON AFTER REACHING 1000 FT CLIMB AGL FEEL DIFF PRESS AND SPEED TRIM FAIL ANNUNCIATOR LIGHTS ILLUMINATED, ELEVATOR CONTROL WAS MARGINALLY HEAVY, AND AUTO PILOT WOULD NOT MAINTAIN PITCH CONTROL. : R&R ELEVATOR FEEL COMPUTER IAW B737 AMM 22-31-37 PARA 2A AND 27-31-37 PARA 3 G (11) AND B737 AMM 27-31-00 PARA 16A THROUGH AND INCLUDING 27-31-00 PARA 16 F (4)(D). R&R ELEVATOR FEEL POSITION SENSOR IAW B737 AMM 22-11-30.

Source: SDR K11A2024081300277 · FAA SDRS
F · 2024-07-16 Matched by certificate designator
ATA 2780

PROBLEM DESCRIPTION: TRAILING EDGE FLAP ASYMMETRY LEFT FLAP INDICATE UP & RIGHT FLAP INDICATES L1, SLATS DID NOT EXTEND WHEN FLAP HANDLE WAS MOVED TO #1 DETENT. CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: FOUND #3 FLAP TRANSMISSION TORQUE TUBE COUPLING DISENGAGED. INSPECTED TORQUE TUBE IAW B737 AMM 27-51-00. RE-ENGAGED AND SECURED TORQUE TUBE COUPLING IAW B737 AMM 27-57-64, PERFORMED OPS CHECK OF TRAILING EDGE FLAP SYSTEM IAW B737 AMM 27-51-00 OPS CHECK GOOD.

Source: SDR K11A2024071600269 · FAA SDRS
O · 2024-01-26 Matched by certificate designator
ATA 5347

AFT CARGO COMPARTMENT B.S 727D RBL 14 HAS CRACK ON TRACK TIE DOWN LWR LEG.

Source: SDR K11A2024020200257 · FAA SDRS
O · 2024-01-15 Matched by certificate designator
ATA 5310

EVIDENCE OF CORROSION ON UPPER WEB AROUND NUTPLATES AT APROX STA 1104 INSIDE LH TORQUE BOX.

Source: SDR K11A2024022600259 · FAA SDRS
O · 2024-01-15 Matched by certificate designator
ATA 5753

LH WING IB AFT FLAP IB SECTION HAS DELAMINATION.

Source: SDR K11A2024012400252 · FAA SDRS
O · 2024-01-10 Matched by certificate designator
ATA 5347

AFT CARGO COMPARTMENT AT B.S. 727D RBL 14, EVIDENCE OF CORROSION AT CARGO TIE DOWN.

Source: SDR K11A2024020200256 · FAA SDRS
O · 2023-12-05 Matched by certificate designator
ATA 5414

#1 PYLON HAS EVIDENCE OF CORROSION ON TOP SIDE

Source: SDR K11A2024012500253 · FAA SDRS
O · 2023-12-05 Matched by certificate designator
ATA 5410

#2 PYLON HAS EVIDENCE OF CORROSION ON TOP SIDE

Source: SDR K11A2024012500254 · FAA SDRS
J · 2023-06-22 Matched by certificate designator
ATA 2750

DURING FLIGHT LE FLAP TRANSIT LIGHT ILLUMINATED (#5 LE LIGHT)

Source: SDR K11A2023062200214 · FAA SDRS
W · 2022-12-15 Matched by certificate designator
ATA 5100

DURING TAXI AT KCVG THE AIRCRAFT DEPARTED THE PAVED SURFACE. DURING RECOVERY THE AIRCRAFT WAS DAMAGED BY SUPPORT EQUIPMENT. DAMAGE IS LOCATED ON THE AFT FUSELAGE JUST FORWARD OF THE AFT LOWER CARGO DOOR. CORRECTIVE ACTION FOR THE REPAIR WILL BE LOGGED AFTER THE COMPLETION OF THE REPAIRS AS A STRUCTURAL DAMAGE REPORT.

Source: SDR K11A2022121500173 · FAA SDRS
J · 2021-11-09 Matched by certificate designator
ATA 2312

PROBLEM DESCRIPTION: NUMBER 1 VHF COM NOT TRANSMITTING. CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: SWAPPED #1 AND #2 VHF COM R/T IAW KCII GMM CHAPTER 1, TRANSFERRED TO DMI # 73400055 IAW KCII B737 MEL 23-3A CAT C DUE 11-19-2021 PLACARDS INSTALLED. REF CLEARING OF DMI #73400055. CLEARED ON LOG PAGE 737-001-5676 R&R VHF R/T IAW B737 AMM 23-21-21 OPS CHECK GOOD IAW B737 AMM 23-21-01 THIS CLEARS DMI 73400055 PLACARDS REMOVED.

Source: SDR K11A2021110900083 · FAA SDRS
O · 2021-10-01 Matched by certificate designator
ATA 5230

UNABLE TO PRESSURIZE IN AUTO OR STANDBY. CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: FOUND AFT CARGO DOOR SLIGHTLY OPEN, ADJUSTED AFT CARGO DOOR IAW B737 AMM 53-11-00. CARGO DOOR CHECK GOOD, PERFORMED OPS CHECK AND LEAK CHECK OF PRESSURIZATION SYSTEM IAW B737 AMM 21-31-00, NO DEFECTS NOTED

Source: SDR K11A2021100100080 · FAA SDRS
G · 2021-01-06 Matched by certificate designator
ATA 3400

CO PILOT STATIC INSTRUMENT AS WELL AS TRANSPONDER FAILED ON TAKEOFF. CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: PERFORMED OPERATIONS CHECK OF THE NR 2 EFIS SYSTEM, IRU SYSTEM, DADC AND ATC SYSTEM, IAW B737 AMM 34-22-00, 34-28-01, 34-12-01 AND 34-53-02. ALL SYSTEMS OPERATIONS CHECK GOOD, NO DEFECTS NOTED AT THIS TIME.

Source: SDR K11A2021010600035 · FAA SDRS
P · 2020-12-07 Matched by certificate designator
ATA 2751

FLAPS FAILED TO EXTEND PAST 15 DEGREES ON LANDING APPROACH. CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: R & R TRAILING EDGE FLAP POSITION INDICATOR, IAW B737 AMM 27-58-41. ALL OPERATIONS CHECKS GOOD NO DEFECTS NOTED.

Source: SDR K11A2020120700033 · FAA SDRS
O · 2020-07-31 Matched by certificate designator
ATA 5330

DRAIN MAST MATING SKIN SURFACE HAS CORROSION @ #2 & #4 MOUNTING HOLES LOCATED @ STA 986 - 1006 BETWEEN STR 26L & 25L

Source: SDR K11A202008031006 · FAA SDRS
J · 2020-07-02 Matched by certificate designator
ATA 7320

DURING TAKEOFF, NR 1 ENGINE HIT 965 DEG. FOR 3 SECONDS UNTIL PULLED BACK. ENGINE WAS REMOVED AND SENT FOR A SHOP VISIT DURING SHOP VISIT, R & R THE EGT HARNESS, RERIGGED THE VSV, AND R & R THE MEC, ENGINE WAS REINSTALLED AND PAST ALL TESTS

Source: SDR K11A202007028002 · FAA SDRS
M · 2020-07-02 Matched by certificate designator
ATA 7200

DURING TAKEOFF NR 1 ENGINE HIT 965 DEG. FOR 3 SECONDS UNTIL PULLED BACK. PERFORMED VISUAL INSPECTION OF NR 1 ENGINE INLET AND EXHAUST, NO DEFECTS NOTED AND PERFORMED BORESCOPE INSPECTION OF THE HTP BLADES AND THE 1ST STAGE LPT BLADES IAW AMM 72-00-00, NO DEFECTS NOTED, A/C FOUND TO BE SUITABLE FOR NON-REVENUE FLIGHT TO OSC IAW AMM 72-00-00. FURTHER INSPECTION IN PROGRESS IN KOSC.

Source: SDR K11A2020070600002 · FAA SDRS
L · 2020-04-11 Matched by certificate designator
ATA 3350

DURING A CHECK FOUND R1 & L1 DOOR EMERGENCY LIGHTING INOP

Source: SDR K11A2020041101 · FAA SDRS
N · 2019-11-27 Matched by certificate designator
ATA 3260

ON GEAR RETRACTION RIGHT MAIN GEAR UNSAFE LIGHT REMAINED ILLUMINATED. CORRECTIVE ACTION: R&R RIGHT MAIN GEAR UPLOCK PROXIMITY SWITCH IAW AMM 32-61-21, PERFORMED OPS CHECK AND GEAR SWING IAW AMM 32-61-21

Source: SDR K11A2019112977401 · FAA SDRS
J · 2019-11-15 Matched by certificate designator
ATA 2131

DURING CLIMB OUT AT 14,000 FT CABIN PRESSURE GOES TO 10,000 FT IN STAND BY AND AUTO MODES

Source: SDR K11A2019111573401 · FAA SDRS
O · 2019-10-22 Matched by certificate designator
ATA 3210

UPON LANDING RIGHT HAND MAIN LANDING GEAR TORSION LINK BROKE, CORRECTIVE ACTION & OTHER PERTINENT INFORMATION: R&R THE MAIN LANDING GEAR UPPER AND LOWER TORSION LINK, TORSION LINK PIN, LEFT HAND SHIMMY DAMPER, #3 & #4 MWA, #3 BRAKE LINE, #4 BRAKE LINE AND NUMBER 3 BRAKE. PERFORMED MAIN GEAR DAMPER TEST / INSPECTION, NO DEFECTS NOTED.

Source: SDR K11A2019102273401 · FAA SDRS
N · 2019-03-20 Matched by certificate designator
ATA 2697

ON CLIMB OUT AT 8000 FEET THE CAPT AND FO RED MAIN CARGO SMOKE ANNUNCIATOR LIGHTS ILLUMINATED ON THE BOTTOM FWD INSTRUMENT PANEL AS WELL AS THE NR 5 SMOKE DETECTOR LIGHT ON THE AFT OVERHEAD PANEL. CORRECTIVE ACTION: FOUND LOOSE CONNECTOR ON NR 5 MAIN DECK SMOKE DETECTOR. RE SECURED CONNECTOR, OPS CHECK GOOD IAW AEI MM 26-19-01, NO DEFECTS NOTED.

Source: SDR K11A2019032001 · FAA SDRS
O · 2019-01-23 Matched by certificate designator
ATA 3210

UPON LANDING AT KCVG ON RUNWAY 09 AND AT THE TIME OF TOUCHDOWN THE AIRCRAFT SHOOK LEFT TO RIGHT AND PULLED TO THE RIGHT. POST FLIGHT INSPECTION FOUND LEFT MAIN LANDING GEAR SHIMMY DAMPENER MISSING AND TORSION LINK BROKEN AND DAMAGE TO THE HYDRAULIC LINES AND WHEEL ASSY. AIRCRAFT TAXIED UNDER ITS OWN POWER TO ITS PARKING LOCATION. AIRPORT CLOSED RUNWAY UNTIL A FOD CHECK WAS COMPLETED. REPAIR AND CORRECTIVE ACTION IN WORK AT THIS TIME.

Source: SDR K11A2019012301 · FAA SDRS
E · 2018-09-13 Matched by certificate designator
ATA 7250

ON PRE-FLIGHT FOUND DAMAGE TO NR 2 ENGINE TURBINE BLADE. R&R NR 2 ENGINE IAW AMM 71-00-00.

Source: SDR K11A2018091373401 · FAA SDRS
L · 2018-07-28 Matched by certificate designator
ATA 3350

EMERGENCY LIGHT FAIL FUNCTIONAL TEST, LT/RT EMERGENCY BATTERY PACKS

Source: SDR K11A2018100500006 · FAA SDRS
O · 2018-06-27 Matched by certificate designator
ATA 5414

#1 PYLON TOP SIDE APPROX NAC STA 240 HAS CORROSION

Source: SDR K11A2018100373401 · FAA SDRS
O · 2018-05-22 Matched by certificate designator
ATA 5320

FUSELAGE - FLIGHT CREW COMPARTMENT AT APPROX STA 250 LBL 48" EVIDENCE OF CORROSION (JD-50)

Source: SDR K11A2018100505 · FAA SDRS
O · 2018-05-22 Matched by certificate designator
ATA 5320

EVIDENCE OF CORROSION ON AFT PIT FLOOR STRUCTURE AT STA 727A +10 LBL 15

Source: SDR K11A2018100573404 · FAA SDRS
O · 2018-05-22 Matched by certificate designator
ATA 5320

EVIDENCE OF CORROSION ON AFT PIT FLOOR STRUCTURE AT STA 727G RBL 15

Source: SDR K11A2018100573403 · FAA SDRS
O · 2018-03-18 Matched by certificate designator
ATA 5414

NR 1 PYLON TOP SIDE APPROX NAC STA 220 HAS CORROSION, NR 1 PYLON AT W BL 190.00-193.50, NAC 196.84-201.34 (APPROX.) SKIN BLEND DOUBLER

Source: SDR K11A2018100573402 · FAA SDRS